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Cast metal alloys
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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001760
EISBN: 978-1-62708-241-9
Abstract
This article presents a failure analysis of an aluminum cylinder head on an automotive engine. During an endurance test, a crack initiated from the interior wall of a hole in the center of the cylinder head, then propagated through the entire thickness of the component. Metallurgical examination of the crack origin revealed that casting pores played a role in initiating the crack. Stress components, identified by finite element analysis, also played a role, particularly the stresses imposed by the bolt assembly leading to plastic strain. It was concluded that the failure can be prevented by eliminating the bolt hole, using a different type of bolt, or adjusting the fastening torque.
Book Chapter
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001781
EISBN: 978-1-62708-241-9
Abstract
A commercial hybrid-iron golf club fractured during normal use. The club fractured through its cast aluminum alloy hosel. Optical analysis revealed casting pores through 20% of the hosel thickness. Mechanical properties were determined from characterization results, then used to construct a finite element model to analyze material performance under failure conditions. In addition, a full scale structural test was conducted to determine failure strength. It was concluded that the club failed not from ground impact but from a force reversal at the bottom of the downswing. Large moments generated during the downswing aggravated by manufacturing defects and stress concentration combined to create an overload condition.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048423
EISBN: 978-1-62708-226-6
Abstract
The bone cement failed at the distal end of the prosthesis stem of femoral head prosthesis six months after implantation. A small indentation on the lateral contour of the stem was visible where the stem had broken. The degree of loosening (gap between the lateral stem contour and the bone or cement) and implant loading was revealed by the dislocation of fragments of the prosthesis. Secondary cracks that had originated at the lateral aspect of the stem were revealed by metallographic examination of a section parallel to the stem surface and perpendicular to the fracture surface of the distal fragment. Gas pores are apparent in the grain and at the grain boundaries were revealed by a transverse section. Fine parallel line structures that run diagonally through the fractograph may be slip traces were revealed by scanning electron microscopy. One of the cracks was revealed to have propagated through a larger gas pore by a ruptured gas pore. The stresses created through the fatigue process activated glide systems which served the formation of secondary cracks along glide planes.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001708
EISBN: 978-1-62708-217-4
Abstract
The paper describes the findings from a damaged propeller blade made from Mn-Ni-Al-bronze, commercially known as Superston 70 (ABS Type 5). The blade had broken at the 0.65 pitch radius location, and the fracture occurred in a brittle mode. The findings reported here point to two potential contributors to the propeller blade failure, viz., the presence of casting flaws at the low pressure side of the propeller blade and service stresses at this surface that reached approximately 400 MPa. This stress value exceeded the yield strength at the corresponding location of the unbroken blade by approximately 40%.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0046142
EISBN: 978-1-62708-217-4
Abstract
To ensure no malfunctions and although there were no apparent problems, a main fuel control was returned to the factory for examination after service on a test aircraft engine that had experienced high vibrations. When the fuel control was disassembled, a lever, cast from AMS 5350 (AISI type 410) stainless steel that was through-hardened to 26 to 32 HRC and passivated, was shown to be cracked. The crack initiated at the sharp corner of the elongated milled slot and propagated across to the outer wall. The sections around the crack were spread about 30 deg apart, showing the fracture surface under investigation had beach marks initiating at the sharp corner along the milled slot. Changes in frequency or amplitude of vibration caused different rates of propagation, resulting in a change in pattern. This evidence supported the conclusion that the lever failed in fatigue as a result of excessive vibration of the fuel control on the test engine. Recommendations included redesign of the lever with a large radius in the corner where cracking originated. This would reduce the stress-concentration factor significantly, thus minimizing the susceptibility of the lever to fatigue.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0089563
EISBN: 978-1-62708-217-4
Abstract
A lever (machined from a casting made of AISI type 410 stainless steel, then surface hardened by nitriding) that was a component of the main fuel-control linkage of an aircraft engine fractured in flight after a service life of less than 50 h. Investigation (radiographic inspection) supported the conclusions that the lever broke at a cold shut extending through approximately 95% of the cross section. The normally applied load constituted an overload of the remainder of the lever. Recommendations included adding magnetic-particle inspection to the inspection procedures for this cast lever.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006421
EISBN: 978-1-62708-217-4
Abstract
Cracks were found on the wing leading edge of a test aircraft made from AZ31B magnesium alloy. Crack lengths were approximately 230 mm (9 in.) long on the left side and approximately 130 mm (5 in.) long on the right side. The cracks ran parallel to the leading edge. The 230-mm (9-in.) crack was received for examination. Visual examination of the submitted panel revealed two cracks. One crack ran through six adjacent fastener holes. Sections of the beveled edges of the holes were missing and corrosion was evident. Visual examination of the fastener holes after separation of the crack showed that the fracture faces were corroded. Optical examination of either side of the middle group of fastener holes showed that the area of suspected crack initiation had suffered excessive corrosion. Examination of the holes on the end of the crack showed fracture characteristics typical of fatigue and/or corrosion fatigue. It was concluded that crack propagation of the fracture in the wing panel occurred by a combination of corrosion and high-cycle fatigue in the end fastener holes. It was recommended that future panels be manufactured of 2024 aluminum.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001222
EISBN: 978-1-62708-225-9
Abstract
A full lift disk, made of die cast brass, which served as a lifting aid in a safety valve, had cracked in service at a number of locations in the vicinity of the threaded hole. During microscopic examination, agglomeration of oxide inclusions were noted in the region of the cracks. Because the die cast brass was alloyed with aluminum, these inclusions consisted predominantly of aluminum oxide. The tolerable limit in pores and oxide inclusions was greatly exceeded in the lift disk under examination. Above all, the numerous oxide skins disrupted the cohesion of the microstructure and were primarily responsible for the failure of the lift disk.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001530
EISBN: 978-1-62708-225-9
Abstract
This paper describes an investigation on the failure of a large leaded bronze bearing that supports a nine-ton roller of a plastic calendering machine. At the end of the normal service life of a good bearing, which lasted for seven years, a new bearing was installed. However the new one failed catastrophically within a few days, generating a huge amount of metallic wear debris and causing pitting on the surface of the cast iron roller. Following the failure, samples were collected from both good and failed bearings. The samples were analyzed chemically and their microstructures examined. Both samples were subjected to accelerated wear tests in a laboratory type pin-on-disk apparatus. During the tests, the bearing materials acted as pins, which were pressed against a rotating cast iron disk. The wear behaviors of both bearing materials were studied using weight loss measurement. The worn surfaces of samples and the wear debris were examined by light optical microscope, SEM, and energy-dispersive x-ray microanalyzer. It was found that the laboratory pin-on-disk wear data correlated well with the plant experience. It is suggested that the higher lead content ~18%) of the good bearing compared with 7% lead of the failed bearing helped to establish a protective transfer layer on the worn surface. This transfer layer reduced metal-to-metal contact between the bearing and the roller and resulted in a lower wear rate. The lower lead content of the failed bearing does not allow the establishment of a well-protected transfer layer and leads to rapid wear.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001522
EISBN: 978-1-62708-235-8
Abstract
In the EMD-2 Joint Directed Attack Munition (JDAM), the A357 aluminum alloy housing had been redesigned and cast via permanent mold casting, but did not meet the design strength requirements of the previous design. Mechanical tests on thick and thin sections of the forward housing assembly revealed tensile properties well below the allowable design values. Radiology and CT evaluations revealed no casting defects. Optical microscopy revealed porosity uniformly distributed throughout the casting on the order of 0.1 mm pore diam. Scanning electron microscopy revealed elongated pores, which indicated turbulent filling of the mold. Spherical pores would have indicated the melt had been improperly degassed. Based on these findings, it was recommended that the manufacturer analyze and redesign the gating system to eliminate the turbulent flow problem during the permanent mold casting process.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001640
EISBN: 978-1-62708-235-8
Abstract
A new supplier for aluminum die castings was being evaluated, and the castings failed to meet the durability test requirements. Specifically, the fatigue life of the castings was low. Initial inspection of the fatigue fracture surfaces revealed large-scale porosity visible to the naked eye. New castings with reduced porosity also failed the durability tests. The fatigue fracture surfaces of additional casting fragments were very rough and contained multiple ratchet marks along the inner fillet. These observations indicated the fatigue process was heavily influenced by the presence of surface imperfections. Improving the surface finish or choosing a stronger alloy, were more likely to improve part durability than reducing the porosity.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001908
EISBN: 978-1-62708-235-8
Abstract
Cluster bomb tailcone assemblies each containing two aluminum die-cast components were rejected because of the poor surface condition of the die castings. Numerous heat checks were found on the surfaces of the tailcones and radiographic inspection revealed inclusions, gas holes, and shrinkage defects in the castings. Most of the components failed to meet required mechanical properties because of these casting defects.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001543
EISBN: 978-1-62708-218-1
Abstract
To determine the effect of severe service on cast 357 aluminum pistons, a metallurgical evaluation was made of four pistons removed from the engine of the Hawk-Offenhauser car which had been driven by Rich Muther in the first Ontario, California 500 race. The pistons were studied by visual inspection, hardness traverses, radiography, dye penetrant inspection, chemical analysis, macrometallography, optical microscopy, and electron microscopy. The crown of one piston had a rough, crumbly deposit, which was detachable with a knife. Two pistons had remains of carbonaceous deposits. The fourth was severely hammered. It was concluded that the high temperatures developed in this engine created an environment too severe for 357 aluminum. Surfaces were so hot that the low-melting constituent melted. Then, the alloy oxidized rapidly to form Al2O3, an abrasive which further aggravated problems. The temperature in much of the piston was high enough to cause softening by overaging, lowering strength.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0046737
EISBN: 978-1-62708-229-7
Abstract
After 14 months of service, cracks were discovered in castings and bolts used to fasten together braces, posts, and other structural members of a cooling tower, where they were subjected to externally applied stresses. The castings were made of copper alloys C86200 and C86300 (manganese bronze). The bolts and nuts were made of copper alloy C46400 (naval brass, uninhibited). The water that was circulated through the tower had high concentrations of oxygen, carbon dioxide, and chloramines. Analysis (visual inspection, bend tests, fractographs, 50x unetched micrographs, 100x micrographs etched with H4OH, and 500x micrographs) supported the conclusions that the castings and bolts failed by SCC caused by the combined effects of dezincification damage and applied stresses. Recommendations included replacing the castings with copper alloy C87200 (cast silicon bronze) castings. Replacement bolts and nuts should be made from copper alloy C65100 or C65500 (wrought silicon bronze).
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001566
EISBN: 978-1-62708-229-7
Abstract
A desuperheater diffuser nozzle in the steam supply line failed within nine months of service in an 8.25 MN/sq m (1200 psig) steam line. The nozzle was an austenitic stainless steel casting in conformance to material. The nozzle had numerous cracks on the inside and outside surfaces, and the cracks had penetrated through the wall thickness in several areas. The fracture surfaces had distinct beach markings delineating the crack front, representative of crack propagation stages. The cracks were transgranular and, unlike classical corrosion-fatigue cracks, exhibited branching, characteristic of chloride-induced SCC in austenitic stainless steels. The failure resulted from chloride-induced SCC, possibly assisted by cyclic stress. The recommendation for alternate material for the desuperheater nozzle included nickel base alloys per ASTM B 564, Grades 600 or 800 titanium alloy per ASTM B 367, Grades C3/C4, or ferritic stainless steel alloy per ASTM 182, Grade FXM27.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0046366
EISBN: 978-1-62708-236-5
Abstract
Several large chromium-plated 4340 steel cylinders were removed from service because of deep longitudinal score marks in the plating. One of the damaged cylinders and a mating cast aluminum alloy B850-T5 bearing adapter that also exhibited deep longitudinal score marks were submitted for examination. Analysis (visual inspection, manual testing of the hardness and adherence of the chromium plating, 100x microscopic examination, and hardness testing) supported the conclusions that high localized loads on the cylinder had resulted in chipping of the chromium plating, particles of which became embedded in the aluminum alloy adapter. The sliding action of the adapter with embedded hard particles resulted in scoring of both the cylinder and the adapter. If the cylinder alone had been available for examination, it might have been concluded that the scoring had been caused by entrapped sand or debris from an external source. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001199
EISBN: 978-1-62708-235-8
Abstract
Lakes in zinc die castings are areas encompassed by irregular lines or waves on flat or slightly contoured surfaces which are intended to look uniform. The laked areas have to be removed by polishing before the castings can be plated. This adds considerably to the overall cost of production. Castings examined were of an automobile name-plate holder with two flat sides of approximately 113 sq cm. All castings produced during a trial showed laking defects, the number and position varying from casting to casting. It was found that formation of metal waves and lakes depended primarily on the design of the gate and runner system and operating conditions. High flow efficiencies, with adequate feeding to all sections of the die, and short cavity fill times are desirable.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001439
EISBN: 978-1-62708-235-8
Abstract
Persistent leakage was experienced from copper tube heaters which formed part of dairy equipment. Metallurgical examination of the brazed joints showed them to have suffered a preferential corrosion attack. This resulted in the phosphide phase of the brazing alloy being corroded away, leaving a weak, porous residual structure. The brazing alloy was of type CP 1 as covered by BS 1845. Header and tube materials were basically copper-nickel alloys for which the use of a phosphorus bearing brazing alloy is not recommended owing to the possibility of forming the brittle intermetallic compound, nickel phosphide. The use of a brazing alloy containing phosphorus was unsuitable on two counts and a quaternary alloy containing silver, copper, cadmium and zinc, such as those in group AG1 or AG2 of BS 1845 would be more suitable. However, because corrosive problems experienced in these units indicated severe service conditions, a proprietary alloy similar to AG1, but containing 3% nickel, was recommended.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047453
EISBN: 978-1-62708-235-8
Abstract
The origins of the casting are unknown. It is included here as a classic case of intergranular corrosion. The part (apparently a pump outlet) was named the “rubber casting” because of the severity of the intergranular attack. Every grain boundary has been attacked to the extent that the casting could be twisted and stretched as through made of rubber. The chemistry of the casting was acceptable for CN-7M. The reason the part failed is a continuous film of carbide with a continuous crack running parallel to the carbides. This sensitized structure produces an area depleted in protective chromium, making it susceptible to corrosion. Two solutions to this problem are available. The simplest is to ensure correct heat treatment to dissolve grain-boundary carbide film and return the protective chromium to the depleted zone. Alternatively, a low-carbon (0.03% maximum C, for example, CF-3) grade can be specified. Procedures are given in a reference for screening castings that may be susceptible to intergranular corrosion due to processing errors.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001217
EISBN: 978-1-62708-235-8
Abstract
In a housing made of cast steel GS 20MoV12 3, weighing 42 tons, precipitates were found on the austenitic grain boundaries during metallographic inspection. According to their shape and type they were recognized as carbides that precipitated during tempering. In addition, a much coarser network of rod-shaped and plate-shaped precipitates was found, that probably corresponded to the primary grain boundaries, or to the grain boundaries or twin planes of the austenite formed during solidification of the melt. These particles could have been aluminum nitride judging by their shape and order of precipitation. Tests showed that a subsequent removal of this defect by solutioning was impractical because the annealing temperature was too high. To avoid this defect in the future the sole recommendation is to accelerate the cooling rate through the critical region between 1200 to 900 deg C to such an extent as is practicable with respect to machinability.
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