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Gas turbines
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Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006824
EISBN: 978-1-62708-329-4
Abstract
This article focuses on common failures of the components associated with the flow path of industrial gas turbines. Examples of steam turbine blade failures are also discussed, because these components share some similarities with gas turbine blading. Some of the analytical methods used in the laboratory portion of the failure investigation are mentioned in the failure examples. The topics covered are creep, localized overheating, thermal-mechanical fatigue, high-cycle fatigue, fretting wear, erosive wear, high-temperature oxidation, hot corrosion, liquid metal embrittlement, and manufacturing and repair deficiencies.
Book
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.9781627083294
EISBN: 978-1-62708-329-4
Book Chapter
Corrosion Failures in Gas Turbine Hot Components
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001827
EISBN: 978-1-62708-241-9
Abstract
Gas turbines and other types of combustion turbomachinery are susceptible to hot corrosion at elevated temperatures. Two such cases resulting in the failure of a gas turbine component were investigated to learn more about the hot corrosion process and the underlying failure mechanisms. Each component was analyzed using optical and scanning electron microscopy, energy dispersive spectroscopy, mechanical testing, and nondestructive techniques. The results of the investigation provide insights on the influence of temperature, composition, and microstructure and the contributing effects of high-temperature oxidation on the hot corrosion process. Preventative measures are also discussed.
Book Chapter
Degradation of Thermal Barrier Coated Superalloy Component During Service
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001829
EISBN: 978-1-62708-241-9
Abstract
An investigation was conducted to better understand the time-dependent degradation of thermal barrier coated superalloy components in gas turbines. First-stage vanes are normally subjected to the highest gas velocities and temperatures during operation, and were thus the focus of the study. The samples that were analyzed had been operating at 1350 °C in a gas turbine at a combined-cycle generating plant. They were regenerated once, then used for different lengths of time. The investigation included chemical analysis, scanning electron microscopy, SEM/energy dispersive spectroscopy, and x-ray diffraction. It was shown that degradation is driven by chemical and mechanical differences, oxide growth, depletion, and recrystallization, the combined effect of which results in exfoliation, spallation, and mechanical thinning.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047072
EISBN: 978-1-62708-217-4
Abstract
Postflight inspection of a gas-turbine aircraft engine that had experienced compressor stall revealed that the engine air-intake bullet assembly had dislodged and was seated against the engine-inlet guide vanes at the 3 o'clock position. The bullet assembly consisted of an outer aerodynamic shell and an inner stiffener shell, both of 1.3 mm (0.050 in.) thick aluminum alloy 6061-T6, and four attachment clips of 1 mm (0.040 in.) thick alclad aluminum alloy 2024-T42. Each clip was joined to the outer shell by 12 spot welds and was also joined to the stiffener. Analysis (visual inspection, dye-penetrant inspection, and 10x/150x micrographs of sections etched with Keller's reagent) supports the conclusion that the outer shell of the bullet assembly separated from the stiffener because the four attachment clips fractured through the shell-to-clip spot welds. Fracture occurred by fatigue that initiated at the notch created by the intersection of the faying surfaces of the clip and shell with the spot weld nuggets. The 6061 aluminum alloy shell and stiffener were in the annealed (O) temper rather than T6, as specified. Recommendations included heat treating the shell and stiffener to the T6 temper after forming.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0047986
EISBN: 978-1-62708-217-4
Abstract
The engine on a jet aircraft was shut down immediately as it produced excessive vibration. Complete failure of the cage in one of the two main-shaft ball bearings (placed side by side in the engine) was revealed in the dismantled engine. The ball bearings (made of vacuum-melted 52100 steel) were both of the single-row deep-groove type with split inner rings and were designed to operate at a maximum temperature of 175 deg C. Overtempering of the rings was indicated by the reduced hardness in comparison to unfailed rings. Severe damage to approximately 20% of the load-bearing surface, with more damage on one of the shoulders of the groove, was revealed during examination of the outer raceway of the bearing which indicated misalignment of the bearing. No damage other than spalling cavities in the inner-ring raceway, caused by the elongated subsurface inclusion revealed by metallographic examination of circumferential section of the largest cavity, was exhibited by the second bearing. It was concluded that the fracture of the cage was caused by overheating and misalignment caused excessive stressing of the bearing on the main shaft.
Book Chapter
Probabilistic Damage Tolerance Analysis of Gas Turbine Rotors
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0090030
EISBN: 978-1-62708-217-4
Abstract
A DC-10 in transit from Denver to Chicago experienced failure of the center engine. The titanium compressor disk burst and severed the hydraulics of the plane. Investigation supports the conclusion that the cause of the disk rupture was the presence of a large fatigue crack near the bore emanating from a hard alpha (HA) defect. Such defects can result from occasional upsets during the vacuum melting of titanium. These nitrogen-rich alpha titanium anomalies are brittle and often have associated microcracks and microvoids. A probabilistic damage tolerance approach was recommended to address the anomalies, with the objective of enhancing rotor life management practices. The ongoing work involves the use of fracture mechanics and software (called DARWIN.) optimized for damage tolerant design and analysis of metallic structural components.
Book Chapter
Damage in a Gas Turbine Hot Gas Casing
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001737
EISBN: 978-1-62708-229-7
Abstract
The hot gas casing of a gas turbine used for peak load power production had developed extensive cracking during operation. The operating time was 18,000 h, and it had been subjected to 1,600 operating cycles. The gas temperature on the hot side was 985 deg C, on the cold side 204 deg C, the material being AISI 321 stainless steel. The purpose of the present study was to determine optimum repair welding procedures on the premise that the material was basically sound and undamaged by creep. The cracking was the result of thermal fatigue, and such cracks can propagate at elevated temperature, with damage ahead of the crack tip occurring by means of very local processes of creep. Metallographic examination disclosed heavy surface layers of carbides, such that the material was extremely brittle when subjected to bending. Accordingly, although it was demonstrated that the casing could be welded successfully, it was suggested that the remaining useful life was effectively exhausted and that it should be replaced. Thermal stresses produced during operation would rapidly result in additional cracks.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c9001748
EISBN: 978-1-62708-225-9
Abstract
A pinion gear made of AMS 6470 steel, nitrided all over, lost internal splined teeth due to wear. Spline failure of the power turbine gear caused an engine overspeed and disintegration. Excessive spline wear resulted from a new coupling being mated during overhaul with a worn gear spline. Wear on the spline teeth flanks of the coupling was attributed to severe wear on the mating gear (internal) spline teeth. The assigned cause was an inadequate maintenance procedure which resulted in a wear-damaged component being retained in the power train during engine overhaul. To prevent reoccurrence, specific inspection criteria were issued defining maximum limits for spline wear. A procedure and requirements were specified for installing the coupling and pinion gear at the next overhaul.
Book Chapter
High-Temperature Degradation of a Gas Turbine Transition Duct
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0091754
EISBN: 978-1-62708-229-7
Abstract
A transition duct was part of a 100-MW power-generation gas turbine. The duct was fabricated from several panels of a modified nickel alloy, IN-617. After six years of operation, two such ducts failed during the next two years, causing outages. Failure was in the form of a total collapse of the duct. Carbides and carbonitrides were found in all of the transitions examined. Investigation supported the conclusion that failure was caused by oxidation, oxide penetration, and oxide spallation which caused thinning of the duct wall. It was felt that the high oxygen and nitrogen partial pressures of the gases within the duct, combined with the high temperatures, facilitated nitrogen pickup. No recommendations were made.
Book Chapter
Failure of a Turbine Vane
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0046966
EISBN: 978-1-62708-229-7
Abstract
A turbine vane made of cast cobalt-base alloy AMS 5382 (Stellite 31; composition: Co-25.5Cr-10.5Ni-7.5W) was returned from service after an undetermined number of service hours because of crack indications on the airfoil sections. This alloy is cast by the precision investment method. Analysis (visual inspection, 100x/500x metallographic examination of sections etched with a mixture of ferric chloride, hydrochloric acid, and methanol, and bend tests) supported the conclusions that cracking of the airfoil sections was caused by thermal fatigue and was contributed to by low ductility due to age hardening, subsurface oxidation related to intragranular carbides, and high residual tensile macrostresses. No further conclusions could be drawn because of the lack of detailed service history, and no recommendations were made.
Book Chapter
Failure of Gas Turbine Last- Stage Bucket
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0091761
EISBN: 978-1-62708-229-7
Abstract
Turbine buckets in a 37.5-MW gas turbine made of Udimet 500 superalloy failed in service. The power plant was located 1 km (0.6 miles) from the Pacific Ocean and operated on No. 2 diesel fuel, which was supplied by tanker ship. Turbine bucket failures occurred on three units after 2500 to 6400 h of operation. Investigation (visual inspection, metallographic examination, and stress analysis) supported the conclusion that the differing microstructure of the airfoil resulted in changes in mechanical properties. Because normal operation includes cycling of loads and temperatures, the shroud tip fractured due to thermomechanical fatigue in its degraded state. Recommendations included special chromium or silicon-rich coating to minimize corrosion in gas turbines operating in a marine environment with operating temperatures in the range of type 2 corrosion (650 to 750 deg C, or 1200 to 1380 deg F). Additionally, it was suggested that fuel delivery, handling, and treatment be high quality, to maintain fuel contamination within design limits, and inlet air filtration must be designed for the coastal site. Also, changing the bucket tip by increasing its thickness and changing the casting technique would reduce the stress and make the design more tolerant of corrosion.
Book Chapter
Cracking in a Gas-Turbine Fan-Duct Assembly Because of Contamination of a Repair Weld
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0047645
EISBN: 978-1-62708-229-7
Abstract
An outer fan-duct assembly of titanium alloy Ti-5Al-2.5Sn (AMS 4910) for a gas-turbine fan section cracked 75 mm (3 in.) circumferentially through a repair weld in an arc weld in the front flange-duct segment. Examination of the crack with a binocular microscope revealed no evidence of fatigue. A blue etch-anodize inspection showed the presence of an alpha case along the edges of the repair weld. The alpha case, a brittle oxide-enriched layer, forms when welds are inadequately shielded from the atmosphere during deposition. The brittleness of this layer caused transgranular cracks to form and propagate in tension under the thermal stresses created by the repair-weld heat input. The crack resulted from contamination and embrittlement of a repair weld that had received inadequate gas shielding. Thermal stresses cracked the oxide-rich layer that formed. The gas-shielding accessories of the welding torch were overhauled to ensure that leak-in or entrainment of air was eliminated. Also, the purity of the shielding-gas supplies was rechecked to make certain that these had not become contaminated.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0047681
EISBN: 978-1-62708-229-7
Abstract
A fluorescent liquid-penetrant inspection of an experimental stator vane of a first-stage axial compressor revealed the presence of a longitudinal crack over 50 mm (2 in.) long at the edge of a resistance seam weld. The vane was made of titanium alloy Ti-6Al-4V (AMS 4911). The crack was opened by fracturing the vane. The crack surface displayed fatigue beach marks emanating from the seam-weld interface. Both the leading-edge and trailing-edge seam welds exhibited weld-metal expulsions up to 3.6 mm (0.14 in.) in length. Metallographic examination confirmed that metal expulsion from the resistance welds was generally present. The stator vane failed by a fatigue crack that initiated at internal surface discontinuities caused by metal expulsion from the resistance seam weld used in fabricating the vane. Expulsion of metal from seam welds should be eliminated by a slight reduction in welding current to reduce the temperature, by an increase in the electrode force, or both.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0090114
EISBN: 978-1-62708-229-7
Abstract
The first-stage blades in a model 501D5 gas turbine had 16 cooling holes. After 32,000 h of service, the blades exhibited cracking at the cooling holes. The blade material was wrought Udimet 520 alloy, with nominal composition of 57Ni-19Cr-12Co-6Mo-1W-2Al-3Ti-0.05C-0.005B. The cooling holes' surface was not coated. Investigation supported the conclusions that the cracking at the cooling holes was due to grain-boundary oxidation and nitridation at the cooling hole surface, embrittlement and loss of local ductility of the base alloy, temperature gradient from the airfoil surface to the cooling holes, which led to relatively high thermal stresses at the holes located at the thicker sections of the airfoil, and stress concentration of 2.5 at the cooling hole and the presence of relatively high total strain (an inelastic strain of 1.2%) at the cooling hole surface. Recommendations include applying the specially designed methods given in this case study to estimate the metal temperature and stresses in order to predict the life of turbine blades under similar operating conditions.
Book Chapter
Cracking in Gas Turbine Blades
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0090181
EISBN: 978-1-62708-229-7
Abstract
Cracking in gas turbine blades was found to initiate from a mechanism of low-cycle fatigue (LCF). LCF is induced during thermal loading cycles in gas turbines. However, metallography of two cracked blades revealed a change in microstructure at as-cast surfaces for depths up to 0.41 mm (0.016 in.). Evaluation by SEM confirmed the difference in structure was associated with a lack of formation of coarse gamma prime structure in the matrix. Microhardness and miniature tensile test results indicated lower strength consistent with the absence of the coarse gamma prime constituent. The blade vendor found that the lot of hot isostatically pressed (HIP) blade castings had been exposed to an improper atmosphere during the HIP process, resulting in the weakened structure. Because subsequent failures were found in blades that did not come from the suspect HIP lot, the scope of the problem was considered generic, and the conclusion was that the primary failure mechanism was LCF. Material imperfections were a secondary deficiency that had the effect of causing the blades from the bad HIP lot to crack first.
Book Chapter
Failure Analysis of Gas Turbine Last Stage Bucket Made of Udimet 500 Superalloy
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001602
EISBN: 978-1-62708-229-7
Abstract
This article presents a failure analysis of 37.5 mW gas turbine third stage buckets made of Udimet 500 superalloy. The buckets experienced repetitive integral tip shroud fractures assisted by a low temperature (type II) hot corrosion. A detailed analysis was carried out on elements thought to have influenced the failure process: a) the stress increase from the loss of a load bearing cross-sectional area of the bucket tip shroud by the conversion of metal to the corrosion product (scale), b) influence of the tip shroud microstructure (e.g., a presence of equiaxed and columnar grains, their distribution and orientation), c) evidence of the transgranular initiation, and d) intergranular creep mechanism propagation. The most probable cause of the bucket damage was the combination of increased stresses due to corrosion-induced thinning of the tip shroud and unfavorable microstructures in the tip shroud region.
Book Chapter
Failure Analysis of Gas Turbine Engine Fuel Nozzle Heat Shields
Available to PurchaseSeries: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001508
EISBN: 978-1-62708-236-5
Abstract
New type 321 corrosion-resistant steel heat shields were cracking during welding operations. A failure analysis was performed. The cause was found to be chloride induced stress-corrosion cracking. Packaging was suspected and confirmed to be the cause of the chloride contamination. A contributing factor was the length of time spent in the packaging, 21 years.
Book Chapter
Corrosion Failures of Industrial Refractories and Technical Ceramics
Available to PurchaseSeries: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003551
EISBN: 978-1-62708-180-1
Abstract
This article provides a discussion on the structural ceramics used in gas turbine components, the automotive and aerospace industries, or as heat exchangers in various segments of the chemical and power generation industries. It covers the fundamental aspects of chemical corrosion and describes the corrosion resistance characteristics of specific classes of refractories and structural ceramics. The article also examines the prevention strategies that minimize corrosion failures of both classes of materials.
Book Chapter
Elevated-Temperature Life Assessment for Turbine Components, Piping, and Tubing
Available to PurchaseSeries: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003517
EISBN: 978-1-62708-180-1
Abstract
This article focuses on the life assessment methods for elevated-temperature failure mechanisms and metallurgical instabilities that reduce life or cause loss of function or operating time of high-temperature components, namely, gas turbine blade, and power plant piping and tubing. The article discusses metallurgical instabilities of steel-based alloys and nickel-base superalloys. It provides information on several life assessment methods, namely, the life fraction rule, parameter-based assessments, the thermal-mechanical fatigue, coating evaluations, hardness testing, microstructural evaluations, the creep cavitation damage assessment, the oxide-scale-based life prediction, and high-temperature crack growth methods.
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