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Resistance heating elements
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001238
EISBN: 978-1-62708-232-7
Abstract
Heating elements, consisting of strips, 40 mm x 2 mm, of the widely used 80Ni-20Cr resistance heating alloy, and designed to withstand a temperature of 1175 deg C, were rendered unusable by scaling after a few months service in a through-type annealing furnace, Although the temperature supposedly did not exceed 1050 deg C. Structural observations indicated a special case of internal oxidation. The required conditions for this were apparently provided by the moist hydrogen atmosphere of the annealing furnace, in which the chromium was oxidized, while the oxides of iron and nickel were reduced. Even the carbon suffered incomplete combustion and was enriched in the core. Thus, no protective layer could form or be maintained. The intergranular advancement of the oxidation may have been favored by the precipitation of chromium-rich carbides on the austenite grain boundaries. This form of internal oxidation is, in the case of Ni-Cr alloys, known as green rot. Alloys containing iron should be more resistant. As a preventive measure it was recommended to reduce the operating temperature of the strip sufficiently to allow the use of Fe-Ni-Cr alloys.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001390
EISBN: 978-1-62708-215-0
Abstract
Cracking occurred in type 304L stainless steel sheaths on nichrome wire heaters that had been in storage for about 5 years in a coastal atmosphere. The cracks were discovered when the heater coils were removed from storage in their original polyethylene packing materials and straightened for use. Fractography established that fracture occurred by stress-corrosion cracking. The cracks originated at rusted areas on the cladding that occurred under iron particles left on the surface during manufacture. High hardness values indicated that solution annealing following cold working had not been carried out as specified. It was recommended that the sheathing material be fully annealed and that the outer surface be pickled and passivated.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001106
EISBN: 978-1-62708-214-3
Abstract
Three radiant heating element tubes from an aluminum holding furnace failed after a few months of service. One side of each of the tubes had disintegrated, leaving large holes and thinned cross sections. Microstructural analysis showed that the surface of the tube had been oxidized along the grain boundaries and had extensive precipitation inside the grains. Chemical analysis indicated that the steel used for the tubes was AISI type 316 stainless steel Specifications for the tubes had called for AISI type 310S to be used. It was recommended that other tubes made from the same batch of steel sheet be checked.