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1-6 of 6
Farming machines and farming implements
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0048596
EISBN: 978-1-62708-221-1
Abstract
SAE grade 5 U-bolts were used to fasten auxiliary dual wheels to the axles on a farm tractor. Under typical farm usage, the bolts are expected to have infinite life. However, several U-bolts made of 29 mm diam rod broke after less than 100 h of service. The bolt legs in which the failures occurred were all in the same position relative to the direction of wheel rotation. Visual examination showed the break was a fairly flat transverse fracture in the threaded section between the washer and the nut. The appearance of the fracture surfaces was characteristic of failure by low-cycle fatigue, with a smooth matte fatigue failure region showing beach marks and generally extending over about 40 to 60% of the fracture surface, which indicated severe overload. The point of initiation of fatigue was at the root of the last thread at the edge of the nut on the side toward this washer. The U-bolts fractured in fatigue because the bolt material had poor hardenability relative to the diam of the bolts. The bolt material was changed from 1045 steel to 1527 steel, a warm-finished low-alloy steel. The diameter of the bolts was reduced to 27.2 mm and the threads were rolled rather than cut.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001500
EISBN: 978-1-62708-221-1
Abstract
A ‘worn-out’ spiral bevel gear and pinion set was submitted for examination and evaluation. This was a spiral bevel drive set with the gear attached to a differential. The assembled unit was driving a new, large, experimental farm tractor in normal plowing and tilling operations. The primary failure was associated with the 4820H NiMo alloy steel pinion, and thus the gear was not examined. The mode of failure was rolling contact fatigue, and the cause of failure improper engineering design. The pattern of continual overload was restricted to a specific concentrated area situated diagonally across the profile of the loaded side, which was consistent on every tooth.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001200
EISBN: 978-1-62708-221-1
Abstract
During the operation of tractors with cantilevered body, the lateral wall of the hypoeutectic cast iron cylinder blocks cracked repeatedly. Three of the blocks were examined. The grain structure of the thick-walled part consisted of uniformly distributed graphite of medium flake size in a basic mass of pearlite with little ferrite. But the thin-walled part showed a structure of dendrites of precipitated primary solid solution grains with pearlitic-ferritic structure and a residual liquid phase with granular graphite in the ferritic matrix. The structure was formed by undercooling of the residual melt. In this case, it was promoted by fast cooling of the thin wall and had comparatively low strength. The fracture formation in the cylinder blocks was ascribed primarily to casting stresses. They could be alleviated by better filleting of the transition cross sections. The fracture was promoted by the formation of undercooled microstructure of low strength in the thin-walled part. Similar damage appeared in a cylinder head, in which case, the cracks were promoted by a supercooled structure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001198
EISBN: 978-1-62708-221-1
Abstract
Cast iron bearing caps in tractor engines fractured repeatedly after only short operating periods. The fracture originated in a cast-in groove and ran approximately radially to the shaft axis. The smallest cross section was at the point of fracture. The core structure of the caps consisted of graphite in pearlitic-ferritic matrix. Casting stresses did not play a decisive role because of the simple shape of the pieces that were without substantial cross sectional variations. Two factors exerted an unfavorable effect in addition to comparatively low strength. First, the operating stress was raised locally by the sharp-edged groove, and second, the fracture resistance of the cast iron was lowered at this critical point by the existence of a ferritic bright border. To avoid such damage in the future it was recommended to observe one or more of the following precautions: 1) Eliminate the grooves; 2) Remove the ferritic bright border; 3) Avoid undercooling in the mold and therefore the formation of granular graphite; 4) Inoculate with finely powdered ferrosilicon into the melt for the same purpose; and, 5) Anneal at lower temperature or eliminate subsequent treatment in consideration of the uncomplicated shape of the castings.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001386
EISBN: 978-1-62708-215-0
Abstract
Two type 420 martensitic stainless steel load cell bodies, which had been installed under two of the four legs of a milk storage tank failed in service. The failure occurred near a change in section and involved fracture of the entire cross section. Examination showed a brittle fracture that was preceded by a small fatigue region. Pitting corrosion was evident at the fracture origin. The areas around the load cells had been subjected to regular washdowns using high-pressure hot water, and the pitting was attributed to crevice corrosion between the load cell and the holddown bolts. Prevention of such corrosion by the use of a flexible sealant to eliminate the crevice was recommended.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001039
EISBN: 978-1-62708-214-3
Abstract
The 4140 steel steering spindle on a tricycle agricultural field chemical applicator failed, causing the loss of the front wheel and overturn of the vehicle. The spindle was a solid 120 mm (4.75 in.) diam forging. It had been machined to 115 mm (4.5 in.) in diameter to fit tightly inside a collar at one point and to 90 mm (3.5 in.) for attachment to the steering mechanism at another. Visual examination showed that the spindle fractured at the fillet welds that attached it to the collar. Macrofractography and metallography revealed that the failure initiated at the root of a weld that bridged a wide gap. The most probable cause of failure was improper preheat during welding.