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1-13 of 13
Chromium plating
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.auto.c9001556
EISBN: 978-1-62708-218-1
Abstract
A few Cr-Mo steel piston rods from different production batches were found identically cracked in the eye end near the radius after chrome plating and baking treatment. Two of them cracked in the plating stage itself instantly broke on slight tapping. Cracking initiated from the outer base surface of the forked eye end. The 40 mm diam forged piston rods were subjected to plating after heavy machining on the part without any stress-relieving treatment. Also, time lapses between plating and baking were varied from 3 to 11 h. The brittle cracking along forked eye-end radius portion was attributed to hydrogen embrittlement that occurred during chrome plating.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001520
EISBN: 978-1-62708-235-8
Abstract
Two types of chromium-plated hydraulic cylinders failed by cracking on their outer surfaces. In one case, the parts had a history of cracking in the nominally unstressed, as-fabricated condition. In another, cracks were detected after the cylinders were subjected to a pressure impulse test. Both part types were made of 15-5 PH (UNS S15500) precipitation hardening stainless steel. Hydrogen embrittlement cracking was the likely cause of failure for both part types. Cracking of the as-fabricated parts was ultimately prevented by changing the manufacturing procedure to allow for a reheat treatment. For parts that cracked after pressure testing, excessive dimensional changes precluded the inclusion of a reheat treatment as a manufacturing step, and further failure was averted by carefully employing proper machining practices, avoiding abusive machining.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c9001418
EISBN: 978-1-62708-231-0
Abstract
The crankshaft of a six cylinder, 225-hp diesel engine driving a small locomotive was examined. About nine months after installation a fall in oil pressure was traced to damage to No. 5 crank pin bearing. A small lip present on one side of the discontinuity apparently served to scrape the bearing material. The defect was stoned smooth, a new bearing fitted, and the engine returned to service. The engine performed satisfactorily for a further twelve months until fracture of the crankshaft through the No. 5 crank pin supervened. The fracture revealed a complex torsional fatigue failure. Microscopic examination revealed that the pin had been hard chromium plated and that the plating followed the curved edge of the outer extremity of the defect. This crank pin contained an inherent defect in the form of a slag inclusion or crack situated at the surface. That the crack only showed itself after a period of service suggests that initially it may have been slightly below the surface of the machined pin and some slight extension outwards took place in service.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091378
EISBN: 978-1-62708-219-8
Abstract
A 12.7 mm (0.5 in.) diam tube was removed from a potable water supply due to leaks. The tube wall thickness was 0.711 mm (0.028 in.) with a thin layer of chromium plate on the OD surface. The tube had been in service for approximately 33 years. Investigation (visual inspection, EDS deposit analysis, metallurgical examination, and unetched magnified images) supported the conclusion that failure occurred due to porous material typical of plug-type dezincification initiating from the inside surface. Where the dezincification had progressed through the tube wall, the chromium plate had exfoliated from the base material and cracked. Recommendations included replacing the piping with a more corrosion-resistant material such as red brass (UNS C23000), inhibited Admiralty brass (UNS C44300), or arsenical aluminum brass (UNS C68700).
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0046366
EISBN: 978-1-62708-236-5
Abstract
Several large chromium-plated 4340 steel cylinders were removed from service because of deep longitudinal score marks in the plating. One of the damaged cylinders and a mating cast aluminum alloy B850-T5 bearing adapter that also exhibited deep longitudinal score marks were submitted for examination. Analysis (visual inspection, manual testing of the hardness and adherence of the chromium plating, 100x microscopic examination, and hardness testing) supported the conclusions that high localized loads on the cylinder had resulted in chipping of the chromium plating, particles of which became embedded in the aluminum alloy adapter. The sliding action of the adapter with embedded hard particles resulted in scoring of both the cylinder and the adapter. If the cylinder alone had been available for examination, it might have been concluded that the scoring had been caused by entrapped sand or debris from an external source. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001539
EISBN: 978-1-62708-236-5
Abstract
Overhaul mechanics discovered a crack in an AISI 4340 Cr-Mo-Ni alloy steel pivot bolt when grinding off the chromium plating. The bolt had served for an estimated 10,000 h and was replated when last overhauled. On checking the bolt, several fine cracks were found on the surface. A 6500x micrograph revealed the intergranular nature of a crack. By trying different grinding procedures, investigators were able to reproduce this type of failure in the laboratory. It was concluded that grinding cracks initiated the failure. It should be noted that governing specifications prohibit grinding on high-strength steel; chromium should be stripped by electrochemical methods.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001722
EISBN: 978-1-62708-236-5
Abstract
The crankshaft of a 37.5-hp, 3-cylinder oil engine was examined. The engine had been dismantled for the purpose of a general overhaul and in the course of this work the crankpins were chromium-plated before regrinding. The engine was returned to service and after running for 290 h the crankshaft broke at the junction of the No. 3 crankpin and the crankweb nearest to the flywheel. A typical fatigue crack had originated at a number of points in the root of the fillet to the web. In its early stages it ran slightly into the web but turned back to the pin when it encountered the oil hole. The shaft had been made from a heat-treated alloy steel. The thickness of the plating was approximately 0.025 in. and numerous cracks were visible in it, several of which had given rise to cracks in the steel below. The primary cause of the crankshaft failure was the plating of the crankpins. The presence of the grooves alone would result in considerable intensification of stress in zones which are normally highly stressed, while the crazy cracking introduced a multiplicity of stress-raisers of a type almost ideal from the point of view of initiating fatigue cracks.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.machtools.c9001229
EISBN: 978-1-62708-223-5
Abstract
Two slitting saw blades were delivered for the purpose of determining the cause of damage. One had cracked while the other one came from a prior sheet delivery, that had less tendency to crack formation according to the manufacturer. The blades were supposed to have been stamped out of a sheet made from a 55 kp/sq mm strength steel. The saw blades were used for separating steel profiles at high rotational speeds. The cracks in question were located at the base of the teeth, i.e. at the point of highest operating stress. Metallographic examination showed that all cracks were non-decarburized and were free of chromium deposits. Therefore they could not have existed before heat treatment and chrome plating. It was concluded that the damage was due neither to poor quality of the sheet nor to defective stamping or heat treatment, but had occurred later either during surface treatment or during operation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001540
EISBN: 978-1-62708-217-4
Abstract
Ground maintenance personnel discovered hydraulic fluid leaking from two small cracks in a main landing gear cylinder made from AISI 4340 Cr-Mo-Ni alloy steel. Failure of the part had initiated on the ID of the cylinder. Numerous cracks were found under the chromium plate. A 6500x electron fractograph showed cracking was predominantly intergranular with hairline indications. Leaking had occurred only 43 h after overhaul of the part. Total service time on the part was 9488 h. It was concluded that cracking on the ID was caused by hydrogen embrittlement which occurred during or after overhaul. The specific source of hydrogen which produced failure was not ascertainable.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001552
EISBN: 978-1-62708-217-4
Abstract
This report covers case histories of failures in fixed-wing light aeroplane and helicopter components. A crankshaft of AISI 4340 Ni-Cr-Mo alloy steel, heat treated and nitrided all over, failed in bending fatigue. The nitrided layer was ground too rapidly causing excessive heat generation which induced grinding cracks and grinding burn. Tensional stresses resulting from grinding developed in a thin surface layer. On another crankshaft, chromium plating introduced undesirable residual tensile stresses. Such plating is an unsatisfactory finish for crankshafts of aircraft engines. Aircraft engine manufacturers and aeronautical standards require magnetic particle inspection to detect grinding cracks after reconditioning. Renitriding after any grinding is needed also, regardless of the amount of undersize as it introduces beneficial residual compressive stresses.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001019
EISBN: 978-1-62708-217-4
Abstract
A broken aircraft crankshaft and a severely damaged main brass bearing were examined to determine whether engine failure was initiated in the bearing or in the crankshaft. The steel crankshaft failure was a classical fatigue fracture. The bearing had been subjected to extremely high temperatures, as indicated by melting in the brass components and the extreme distortion in the rollers. Microscopic examination on the crankshaft material showed it to be a good quality steel. On the other hand, the chromium plate was thick, porous, and cracked in many places, including the point of the main fatigue crack. It was concluded that the over-all failure was initiated in the crankshaft, and the failure of the bearing resulted from that failure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c9001507
EISBN: 978-1-62708-217-4
Abstract
A large four-engine aircraft was on a cargo flight at night when a loud bang was heard, accompanied by a loss of power from both engines on the left side. After an emergency landing, it was discovered that the propellers from both left side engines were missing. The initial investigation determined that the four-bladed propeller from the left inboard engine had separated in flight, subsequently impacting the left outboard engine, causing its propeller to separate also. Three years later, the left inboard propeller hub was recovered. All four blades had separated through the shank area adjacent to the hub. Detailed SEM examination confirmed a fatigue mode of failure in this area with a primary single origin on the inside surface of the shank. The main fatigue origin site was coincident with one of the defects on the inner surface of the blade shank. The most probable source for creating the defects on the ID bore of the shank was the blade tip chrome plating process, which was carried out during the last overhaul prior to the failure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001694
EISBN: 978-1-62708-222-8
Abstract
The outer tube, or stem, on a bicycle frame fractured after two years of use. Detailed investigation revealed that the lower stem bearing had been loose for some time and the bottom bearing cup contained many cracks. Metallographic examination of the chromium-plated cup confirmed the brittle nature of the cracks, located along prior austenite boundaries. The failure was attributed to hydrogen embrittlement due to improper manufacturing procedures following chromium plating. The cracking led to looseness in the bearing and consequent scoring, cracking, and overloading of the stem.