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High-speed tool steel
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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001755
EISBN: 978-1-62708-241-9
Abstract
An aero engine failed due to the misalignment of the ball bearing fitted on the main shaft of the engine. The aero engine incorporates two independent compressors: a six-stage axial flow LP compressor and a nine-stage axial flow HP compressor. The bearing under consideration is a HP location bearing and is fitted at the rear of the nine-stage compressor. It was supposed to operate for at least 5000 h, but failed catastrophically after 1300 h, rendering the engine unserviceable. Unusually high stresses caused by misalignment and uneven axial loading resulted in the generation of fatigue crack(s) in the inner race. When the crack reached the critical size, the collar of the race fractured, causing subsequent damage. The cage also failed due to excessive stresses in the axial direction, and its material was smeared on the steel balls and the outer race.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.machtools.c0089429
EISBN: 978-1-62708-223-5
Abstract
The failure of a high speed steel twist drill which caused injury to the user was investigated thoroughly to settle a legal suit. The drill was being used to remove a stud that broke in the vertical wall of a metalworking machine (upsetter) after drilling a pilot hole. The drill had shattered suddenly with a bang which caused a chip to be dislodged and cause the injury. A large nonmetallic inclusion parallel to the axis near the center of the drill was revealed in an unetched longitudinal section. Carbide bands in a martensitic matrix were indicated in an etched sample. It was concluded by the plaintiff's metallurgist that the failed drill was defective as the steel contained nonmetallic inclusions and carbide segregation which made it brittle. It was revealed by the defendant that the twist drill met all specifications of M1 high-speed steel and investigated several other drills without failure to prove that the failure was caused by use in excessive conditions. It was revealed by examination that the point of the broken drill was not the original point put on at manufacture but came from regrinding. Both technical and legal details have been discussed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.machtools.c9001250
EISBN: 978-1-62708-223-5
Abstract
A broken cross-recessed die was examined. Examination of the unetched, polished section for impurities revealed several coarse streaks of slag. The purity did not therefore correspond to the requirements set for a high speed tool steel of the given theoretical quality DMo 5. After etching with 5% nital the polished surface exhibited a pronounced, easily-visible, fibrous structure. Microscopic examination revealed that this etch pattern was produced by marked segregation bands. The very unfavorable structure for a high speed steel tool of these dimensions and subject to such stresses together with the low purity favored the fracture of the tool.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001269
EISBN: 978-1-62708-215-0
Abstract
Recurring, premature failures occurred in TiN-coated M2 gear hobs used to produce carbon steel ring gears. Fractographic and metallographic examination, microhardness testing, and chemical analysis by means of EDS revealed that the primary cause of failure was a coarse cellular carbide network, which created a brittle path for fracture to occur longitudinally. As the cellular carbide network must be dispersed and refined during hot working of the original bar of material, the hobs were not salvageable. Minor factors contributing to the hob failures were premature wear resulting from lower matrix hardness and high sulfur content of the material, which contributed to lower ductility through increased nucleation sites. It was recommended that the hob manufacturer specify a minimum amount of required reduction for the original bar of tool steel material, to provide for sufficient homogenization of the carbides in the resultant hob, and lower sulfur content.