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Ferritic stainless steel
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0048772
EISBN: 978-1-62708-220-4
Abstract
A return bend (made from ASTM A213, grade T11, ferritic steel) from a triolefin-unit heater ruptured after two years in service. The unit operated at 2410 kPa, with a hydrocarbon feed stream (85% propylene) entering at 260 to 290 deg C and leaving at 425 to 480 deg C. The fracture was found to terminate at the welds that joined the bend to the pipeline. A high concentration of both small and large inclusions was exhibited by the metallographic examination of the steel near the fracture. Branched cracks similar to those produced by stress corrosion of steel were observed in a section through the fireside edge of the fracture surface. Scale was observed over most of the crack path which acted as a stress raiser. The effect of the oxide was magnified during thermal cycles because of differential thermal expansion, with the steel having a greater expansion coefficient than the scale. It was recommended that material that is intended for critical applications where failure cannot be tolerated should be non-destructively examined.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0091362
EISBN: 978-1-62708-220-4
Abstract
A nozzle in a wastewater vaporizer began leaking after approximately three years of service with acetic and formic acid wastewaters at 105 deg C (225 deg F) and 414 kPa (60 psig). The shell of the vessel was weld fabricated from 6.4 mm (0.25 in.) E-Brite stainless steel plate and measured 1.5 m (58 in.) in diameter and 8.5 m (28 ft) in length. Investigation (visual inspection, chemical analysis, radiography, dye-penetrant inspection, and hydrostatic testing of all E-Brite welds, 4x images, 100x/200x images electrolytically etched with 10% oxalic acid, and V-notch Charpy testing) supported the conclusion that failure of the nozzle weld was the result of intergranular corrosion caused by the pickup of interstitial elements and subsequent precipitation of chromium carbides and nitrides. Carbon pickup was believed to have been caused by inadequate joint cleaning prior to welding. The increase in the weld nitrogen level was a direct result of inadequate argon gas shielding of the molten weld puddle. Two areas of inadequate shielding were identified: improper gas flow rate for a 19 mm (0.75 in.) diam gas lens nozzle, and contamination of the manifold gas system. Recommendations included changes in the cleaning and welding process.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001692
EISBN: 978-1-62708-229-7
Abstract
Two blade-detachment failures in large (600 kW) wind turbine generators were investigated. In the first case, bolt failures were established as the initial failure event. A fatigue crack reached a critical length, fast fracture developed and was then arrested as the bolt unloaded. Crack growth resumed when loading increased with cracking or fracture of adjacent bolts. The problem was identified as one of insufficient preload on the bolts. In the second failure on a different unit, a retaining nut on a blade assembly split, allowing a roller bearing to slide off a shaft and a blade to separate at its attachment hub. The failure was observed to be by fatigue. It was determined that pieces of the outer retaining rib (or flange) on the bearing inner cage had fractured by fatigue and were trapped between the nut and the bearing, producing excessive cyclic loading on the nut by a wedging action as the blade pitch adjusted during a revolution. Fatigue of the rim occurred as a result of inadequate lubrication in the bearing, which led to load transfer across the rollers, onto the rim.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001412
EISBN: 978-1-62708-229-7
Abstract
Three blades from 45,000 kW, 3,000 rpm turbine were received for examination, comprising the root of blade 28, blade 89 showing a crack in one of the root teeth, and blade 106 which was free from defects. Microscopic examination of the blade material showed it to be a ferritic stainless steel of the type commonly used for turbine blades. A number of non-metallic inclusions were present which had been drawn into threads in rolling; these appeared to consist largely of duplex silicates. The failure of blade 28 was the result of the development of a creeping crack. Magnetic crack examination of blade 89 revealed a crack in a tooth in an identical position to the start of the crack in blade 28 but on the opposite, i.e., steam inlet, side of the blade. Similar examination of blade 106 did not reveal any cracks. Cracking was associated with unsatisfactory bedding of the blade teeth on the faces of the wheel grooves. It was concluded that the blade failures were due primarily to over-loading of the individual blade teeth due to incorrect fitting in the wheel. Vibration was an important contributory factor, as it resulted in the imposition of fluctuating stresses on the overloaded teeth. Non-metallic inclusions in the blade material playing a minor part.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001609
EISBN: 978-1-62708-229-7
Abstract
Alloy 430 stainless steel tube-to-header welds failed in a heat recovery steam generator (HRSG) within one year of commissioning. The HRSG was in a combined cycle, gas-fired, combustion turbine electric power plant. Alloy 430, a 17% Cr ferritic stainless steel, was selected because of its resistance to chloride and sulfuric acid dewpoint corrosion under conditions potentially present in the HRSG low-pressure feedwater economizer. Intergranular corrosion and cracking were found in the weld metal and heat-affected zones. The hardness in these regions was up to 35 HRC, and the weld had received a postweld heat treatment (PWHT). Metallographic examination revealed that the corroded areas contained undertempered martensite. Fully tempered weld areas with a hardness of 93 HRB were not attacked. No evidence of corrosion fatigue was found. Uneven temperature control during PWHT was the most likely cause of failure.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0091048
EISBN: 978-1-62708-235-8
Abstract
A welded ferritic stainless steel heat exchanger cracked prior to service. The welding filler metal was identified as an austenitic stainless steel and the joining method as gas tungsten arc welding. Investigation (visual inspection, SEM images, 5.9x images, and 8.9x/119x images etched with Vilella's reagent followed by electrolytic etching in 10% oxalic acid) supported the conclusion that the heat exchanger cracked due to weld cold cracking or postwelding brittle overload that occurred via flexure during fabrication. The brittle nature of the weld was likely due to a combination of high residual stresses, a mixed microstructure, inclusions, and gross grain coarsening. These synergistic factors resulted from extreme heat input during fillet welding. Recommendations included altering the welding variables such as current, voltage, and travel speed to substantially reduce the heat input.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c0048808
EISBN: 978-1-62708-228-0
Abstract
The welds joining the liner and shell of a fluid catalytic cracking unit failed. The shell was made of ASTM A515 carbon steel welded with E7018 filler metal. The liner was made of type 405 stainless steel and was plug welded to the shell using ER309 and ER310 stainless steel filler metal. Fine cracks starting inside the weld zone and spreading outward through the weld and toward the surface were observed during examination. Decarburization and graphitization of the carbon steel at the interface was noted. The high carbon level was found to allow martensite to form eventually. The structure was found to be austenitic in the area where the grain-boundary precipitates appeared heaviest. The composition of the precipitates was analyzed using an electron microprobe to reveal presence of sulfur. Microstructural changes in the weld alloy at the interface were interpreted to be caused by dilution of the alloy and the presence of sulfur caused hot shortness. The necessary internal stress to produce extensive cracking was produced by the differential thermal expansion of the carbon and stainless steels. Periodic careful gouging of the affected areas followed by repair welding was recommended.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c0065826
EISBN: 978-1-62708-233-4
Abstract
The wires used in a wet precipitator for cleaning the gases coming off a basic oxygen furnace failed. The system consisted of six precipitators, three separate dual units, each composed of four zones. Each zone contained rows of wires (cold drawn AISI 1008 carbon steel) suspended between parallel collector plates. It was determined that the 1008 wires failed because of corrosion fatigue. It was decided to replace all of the wires in the two zones with the highest rates of failure with cold-drawn type 304 austenitic stainless steel wire. These expensive wires, however, failed after a week by transgranular SCC. Annealed type 430 ferritic stainless steel was subsequently suggested to prevent further failures.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001703
EISBN: 978-1-62708-227-3
Abstract
This paper describes the metallurgical investigation of a broken spindle used to attach an antenna to the mast of a naval vessel. Visual inspections of both failed and intact fastener assemblies were carried out both on-board ship and in the laboratory followed by metallographic and fractographic examinations. Simulations were also performed on stressed material in a suitable environment to assess the relative importance of postulated failure mechanisms. Factors contributing to this failure including assembly procedures and applied preloads, service loading and environment, and material selection and specification. The discussion considers whether this failure was an isolated incident or is likely to be a fleet-wide problem, and suggests ways to prevent reoccurrence.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001233
EISBN: 978-1-62708-232-7
Abstract
High-chromium steel pipes 42.25 x 3.25 mm from a blast furnace gas fired recuperator for the preheating of air were heavily oxidized and perforated in places. It was found that the blast furnace gas had a high sulfur content. Both the carburization and the formation of sulfide proved that in addition, from time to time at least, combustion was incomplete and the operation was carried out in a reducing atmosphere, with the result that oxygen deficiency prevented the formation or maintenance of a protective surface layer on the external surface of the pipes. The sulfur would probably not have damaged the nickel-free steel used here at the given temperatures if it had been present as sulfur dioxide in an oxidizing atmosphere. The damage was therefore caused primarily by an incorrectly conducted combustion process.
Series: ASM Handbook Archive
Volume: 11
Publisher: ASM International
Published: 01 January 2002
DOI: 10.31399/asm.hb.v11.a0003553
EISBN: 978-1-62708-180-1
Abstract
This article commences with a discussion on the characteristics of stress-corrosion cracking (SCC) and describes crack initiation and propagation during SCC. It reviews the various mechanisms of SCC and addresses electrochemical and stress-sorption theories. The article explains the SCC, which occurs due to welding, metalworking process, and stress concentration, including options for investigation and corrective measures. It describes the sources of stresses in service and the effect of composition and metal structure on the susceptibility of SCC. The article provides information on specific ions and substances, service environments, and preservice environments responsible for SCC. It details the analysis of SCC failures, which include on-site examination, sampling, observation of fracture surface characteristics, macroscopic examination, microscopic examination, chemical analysis, metallographic analysis, and simulated-service tests. It provides case studies for the analysis of SCC service failures and their occurrence in steels, stainless steels, and commercial alloys of aluminum, copper, magnesium, and titanium.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001324
EISBN: 978-1-62708-215-0
Abstract
A type 430Ti stainless steel flue gas expansion joint cracked because of caustic-induced stress-corrosion cracking. Energy-dispersive X-ray spectroscope analysis of the fracture surface deposits revealed the presence of sodium and potassium—caustics in hydroxide form. Primary fracture surfaces were all similar in appearance, and a primary crack origin could not be identified. A secondary crack brought to fracture in the laboratory showed brittle, cleavage features rather than classic, tensile overload features. This suggested that the material was embrittled.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001047
EISBN: 978-1-62708-214-3
Abstract
An E-Brite /Ferralium explosively bonded tube sheet in a nitric acid condenser was removed from service because of corrosion. Visual and metallographic examination of tube sheet samples revealed severe cracking in the heat-affected zone between the outer tubes and the weld joining the tube sheet to the floating skirt. Cracks penetrated deep into the tube sheet, and occasionally into the tube walls. The microstructures of both alloys and of the weld appeared normal. Intergranular corrosion characteristic of end-grain attack was apparent. A low dead spot at the skirt / tube sheet joint allowed the Nox to condense and subsequently reboil. This, coupled with repeated repair welding in the area, reduced resistance to acid attack. Intergranular corrosion continued until failure. Recommendations included changing operating parameter inlet to prevent HNO3 condensation outside the inlet and replacement of the floating skirt with virgin material (i.e., material unaffected by weld repairs).
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001130
EISBN: 978-1-62708-214-3
Abstract
The failure during use of a seat on a heavy-duty swing set at an elementary school was investigated. The seat contained a perforated reinforcing sheet metal (galvanized type 430 stainless steel) insert covered by an elastomeric material. Specimens of the reinforcing sheet from the failed seat were examined using SEM fractography, tensile and ductility tests, and spectrographic chemical analysis. The test results showed that the steel used did not meet the manufacturer's specifications for ductility (elongation). In addition, the small-diameter punched holes caused a stress concentration factor that aggravated the brittleness of the steel.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001074
EISBN: 978-1-62708-214-3
Abstract
A cast housing, part of a multi-shaft yoking mechanism, failed during assembly and installation of the equipment in which it was to be used. The housing, or yoke body, was cast from AISI 420 grade ferritic stainless steel. Analysis revealed that the failure was caused by the presence of shrinkage cavities, which lowered the load-bearing capability. The failure occurred at the location where there was an abrupt change in the section thickness. A redesign to provide a smooth contour at the section junction was recommended along with optimization of casting parameters to avoid shrinkage cavities.