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Gray iron
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Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006831
EISBN: 978-1-62708-329-4
Abstract
The information provided in this article is intended for those individuals who want to determine why a casting component failed to perform its intended purpose. It is also intended to provide insights for potential casting applications so that the likelihood of failure to perform the intended function is decreased. The article addresses factors that may cause failures in castings for each metal type, starting with gray iron and progressing to ductile iron, steel, aluminum, and copper-base alloys. It describes the general root causes of failure attributed to the casting material, production method, and/or design. The article also addresses conditions related to the casting process but not specific to any metal group, including misruns, pour shorts, broken cores, and foundry expertise. The discussion in each casting metal group includes factors concerning defects that can occur specific to the metal group and progress from melting to solidification, casting processing, and finally how the removal of the mold material can affect performance.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047297
EISBN: 978-1-62708-235-8
Abstract
Door-closer cylinder castings manufactured of class 30 gray iron were breaking during machining. The manufacturing source reported that a random sampling of castings from this lot had hardnesses from 180 to 210 HRB. Based on the color of the components, heat treatment of these castings was suspected. Metallurgical examination on two representative castings supported the conclusions that the cracks in these gray iron door closers that were present either before or during the heat treatment were attributed to a substandard microstructure of the wrong type of graphite combined with excessive ferrite. This anomalous structure is caused by shortcomings in the foundry practice of chemical composition, solidification, and inoculation control. Judging from the microstructure, the strength of the material was lower than desired for class 30 gray iron, and the suspected heat treatment further reduced the strength. Recommendations included that the chemistry and inoculation should be controlled to produce type A graphite structure. The chemistry control should aim for a carbon equivalent close to 4.3% to achieve adequate fluidity for thin sections and to alleviate gas defects.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0048804
EISBN: 978-1-62708-230-3
Abstract
Several cases of failures in gray cast iron paper machine dryer rolls were evaluated. The rolls were found have ground outer cylindrical surfaces on which the paper web is dried. They were found to rotate about their longitudinal axes at speeds from 50 to 250 rpm while containing saturated steam from 35 to 380 kPa. Failures were found to occur in the shell body, in a head near a hand hole or a manhole opening, or in a head near the journal-to-head interface. A cleavage fracture was revealed by scanning electron microscopy regardless of the driving stress for failure. Fracture surface were found to exhibit chevron marks typical of fatigue or raised points or tears pointing in the direction of the probable origin of failure. The characteristics of the thinwall cast iron structures like the variation in composition due to pouring from multiple ladles, variation in solidification rates, and variation in tensile strength to be noted during inspection were described.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0089567
EISBN: 978-1-62708-230-3
Abstract
A paper drier head manufactured from gray cast iron was removed from service as a result of NDE detection of crack-like surface discontinuities. This component was subjected to internal steam pressure to provide heat energy for drying. Investigation (visual inspection, chemical analysis, mechanical testing, as-polished 54x magnification, etched with nital 33x/54x/215x/230x magnification) supported the conclusions that the NDE indications were the consequence of a cold-shut condition in the casting. The cold shut served as a stress-concentration site and was therefore a potential source of crack initiation. The combination of low material strength and a casting defect was a potential source of unexpected fracture during service, because the component was under pressure from steam. Recommendations included removing other dryer heads exhibiting similar discontinuities and/or material quality from service.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.rail.c0047328
EISBN: 978-1-62708-231-0
Abstract
Cracks formed on cylinder inserts from a water-cooled locomotive diesel engine, on the water side in the neck between the cylindrical part and the collar. Cracks were revealed by magnetic-particle inspection. As a rule, several parallel cracks had appeared, some of which were very fine. The part played by corrosion in the formation of the cracks was demonstrated with the help of metallographic techniques. The surface regions of the cracks widened into funnel form, which is a result of the corrosive influence of the cooling water. Actual corrosion pits could not be found indicating that the vibrational stresses had a greater share in the damage than the corrosive influence. Cracks appeared initially only in those engines in which no corrosion inhibitor had been added to the cooling water. The cracking was caused by corrosion fatigue. The combined presence of a corrosive medium and cyclical operating stress was needed to cause cracks. No cracks appeared when corrosion inhibitor was added to the cooling water.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0047335
EISBN: 978-1-62708-219-8
Abstract
A section of cast iron water main pipe contained a hole approximately 6.4 x 3.8 cm (2.5 x 1.5 in.). The pipe was laid in clay type soil. Examination revealed severe pitting around the hole and at the opposite side of the outside diam. A macroscopic examination of a pipe section at the hole area showed that the porosity extended a considerable distance into the pipe wall. Metallographic examination revealed a graphite structure distribution expected in centrifugally cast iron with a hypoeutectic carbon equivalent. Chemical analyses of a nonporous sample had a composition typical of cast iron pipe. Chemical analyses of the porous region had a substantial increase in carbon, silicon, phosphorus, and sulfur. The porous appearance and the composition of the soft porous residue confirmed graphitic corrosion. The selective leaching of iron leaves a residue rich in carbon, silicon, and phosphorus. The high sulfur content is attributed to ferrous sulfide from a sulfate reducing bacteria frequently associated with clay soils. Reinforced coal tar protective coating was recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091384
EISBN: 978-1-62708-219-8
Abstract
A 25.4 cm (10 in.) diam gray cast iron water main pipe was buried in the soil beneath a concrete slab. The installation was believed to have been completed in the early 20th century. A leak from the pipe resulted in flooding of a warehouse. Once removed, the pipe revealed through-wall perforations and cracking along its axis. The perforations and the crack were at the 6 o'clock position. Investigation (visual inspection, radiography, unetched macrographs, and tensile testing) supported the conclusion that the failure occurred as result of years of exposure to ground water in the soil resulting in graphitic corrosion. Soils containing sulfates are particularly aggressive. Recommendations included pipe replacement. The wall thickness had been sufficiently reduced that the pipe could no longer support the required load. Water mains are designed for more than 100 years life. Ductile iron or coated and lined steel pipe, generally not susceptible to graphitic corrosion, were suggested as suitable replacement materials, and cathodic protection was also considered as a possibility.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001226
EISBN: 978-1-62708-234-1
Abstract
A slide and the two guideways of a pump had to be disassembled already during run-in time after approximately 20 h because they had galled completely, before the rated speed of 800 rpm was reached. Chemical analysis of the slide showed the following composition: 3.60C, 3.22Graphite, 2.49Si, 0.51Mn, 0.485P, and 0.112S. The iron was thus distinctly hypereutectic. The galling of the pump parts therefore was favored by an unsuitable structure caused by improper composition and fast cooling. Distortion by casting stresses may have been contributory or may have played the principal part. In order to prevent a repetition, the use of hypoeutectic or eutectic iron, slower cooling of the casting, inoculation of the melt with finely powdered ferrosilicon, and possibly rounding-off the edges or machining of the surfaces are recommended.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0047332
EISBN: 978-1-62708-234-1
Abstract
Deterioration of the vanes and a wearing away of the area surrounding the mainshaft-bearing housing of the pump bowl for a submersible water pump used in a well field were noticed during a maintenance inspection. The bowl was sand cast from gray iron and had been in service approximately 45 months. Visual examination of the vanes and the area surrounding the mainshaft-bearing housing revealed a dark corrosion product that was soft, porous, and of low mechanical strength. There were areas with severe erosion. Macrographs of sections through the pump shell and a vane showed darker areas representing graphitic residue and corrosion products that were not removed by erosion. Exposure of the pump bowl to the well water resulted in graphitic corrosion, which generated a soft, porous graphitic residue impregnated with insoluble corrosion products. Failure of the pump bowl resulted from the continuous erosion of the residue by action of the water within the pump.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001165
EISBN: 978-1-62708-234-1
Abstract
After operating for six months, a pump impeller (of nickel-containing cast iron) showed considerable corrosion. Cross sections showed substantial penetration of the wall thickness without loss of material. The observed supercooled structure implied low strength but would not affect corrosion resistance. Etching of the core structure showed a selective form of cast iron corrosion (spongiosis or graphitic corrosion) which lowered the strength of the cast iron enough that a knife could scrape off a black powder (10.85% C, 1.8% S, 1.45% P). Analysis showed that some of the “sulfate” found in the scrubbing water was actually sulfide (including hydrogen sulfide) and was the main cause of corrosion.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001202
EISBN: 978-1-62708-234-1
Abstract
Two damaged impellers made of austenitic cast iron came from a rotary pump used for pumping brine mixed with drifting sand. On one of the impellers, pieces were broken out of the back wall in four places at the junction to the blades. The fracture edges followed the shape of the blade. Numerous cavitation pits were seen on the inner side of the front wall visible through the breaks in the back wall. The back wall of the as yet intact second impeller which did not show such deep cavitation pits was cracked in places along the line of the blades. The microstructure consisted of lamellar graphite and carbides in an austenitic matrix and was considered normal for the specified material GGL Ni-Cu-Cr 15 6 2. It was concluded that the cause of the damage was porosity at the junction between back wall and blades arising during the casting process. Cavitation did not contribute to fracture but also could have led to damage in the long term in the case of a sound casting. It is therefore advisable in the manufacture of new impellers to take care not only to avoid porosity but also to use alloy GGL Ni-Cu-Cr 15 6 3, which has a higher chromium content and is more resistant to cavitation.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0047220
EISBN: 978-1-62708-220-4
Abstract
Two oil-pump gears broke after four months of service in a gas compressor that operated at 1000 rpm and provided a discharge pressure of 7240 kPa (1050 psi). The compressor ran intermittently with sudden starts and stops. The large gear was sand cast from class 40 gray iron with a tensile strength of 290 MPa (42 ksi) at 207 HRB. The smaller gear was sand cast from ASTM A536, grade 100-70-03, ductile iron with a tensile strength of 696 MPa (101 ksi) at 241 HRB. Analysis (metallographic examination) supported the conclusion that excessive beam loading and a lack of ductility in the gray iron gear teeth were the primary causes of fracture. During subsequent rotation, fragments of gray iron damaged the mating ductile iron gear. Recommendations included replacing the large gear material with ASTM A536, grade 100-70-03, ductile iron normalized at 925 deg C (1700 deg F), air cooled, reheated to 870 deg C (1600 deg F), and oil quenched. The larger gear should be tempered to 200 to 240 HRB, and the smaller gear to 240 to 280 HRB.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.mech.c0047315
EISBN: 978-1-62708-225-9
Abstract
A sand-cast gray iron flanged nut was used to adjust the upper roll on a 3.05 m (10 ft) pyramid-type plate-bending machine. The flange broke away from the body of the nut during service. Analysis (visual inspection and 150x micrographs of sections etched with nital) supported the conclusions that brittle fracture of the flange from the body was the result of overload caused by misalignment between the flange and the roll holder. The microstructure contained graphite flakes of excessive size and inclusions in critical areas; however, these metallurgical imperfections did not appear to have had significant effects on the fracture. Recommendations included carefully and properly aligning the flange surface with the roll holder to achieve uniform distribution of the load. Also, a more ductile metal, such as steel or ductile iron, would be more suitable for this application and would require less exact alignment.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001197
EISBN: 978-1-62708-235-8
Abstract
The front wall of a cast iron crankcase cracked at the transition from the comparatively minor wall thickness to the thick bosses for the drilling of the bolt holes. Metallographic examination showed the case was aggravated by the fact that the casting had a ferritic basic structure and the graphite in part showed a granular formation, so that strength of the material was low. In a second crankcase with the same crack formation the structure in the thick-wailed part was better. But it also showed granular graphite in the ferritic matrix in the thin-walled part between the dendrites of the primary solid solution precipitated in the residual melt. A third crankcase had fractures in two places, first at the frontal end wall and second at the thinnest point between two bore holes. In all three cases casting stresses caused by unfavorable construction and rapid cooling were responsible for the crack formation. A fourth crankcase had cracked in the bore-hole of the frontal face. In this case the cause of the fracture was the low strength of a region that was caused by a bad microstructure further weakened by the bore hole.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.machtools.c0091853
EISBN: 978-1-62708-223-5
Abstract
A 230 mm (9 in.) diameter disk attrition mill was scheduled to grind 6.35 mm (0.25 in.) diameter quartz particles to a 0.075 mm (0.003 in.) diameter powder. Due to severe wear on the grinding plates, however, the unit was unable to complete the task of grinding the rock. The mill consisted of a heavy gray cast iron frame, a gravity feeder port, a runner, and a heavy-duty motor. The frame and gravity feeder weighed over 200 kg (440 lb) and, in some areas, was over 25 mm (1 in.) thick. To obtain the operating speed of 200 rpm, a gear system was used to transmit the torque from the 2-hp motor. The runner consisted of a 50 mm (2 in.) diameter shaft and two gray cast iron grinding plates. Investigation (visual inspection, historical review, photographs, model testing of new plates, chemical analysis, hardness testing, optical macrographs, and optical micrographs) supported the conclusion that the primary feed material was harder than the grinding plates, causing wear and eventual failure. Recommendations included reducing the clearance between the flutes and possible material changes.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c0090938
EISBN: 978-1-62708-221-1
Abstract
Both halves of a gray cast iron transmission housing from a 50-ton dump truck were found to contain numerous cracks. The housing material was possibly G3000 grade designation for automotive gray cast iron. No service duration or material specifications were provided. Investigation (visual inspection, tensile testing, 2% nital etched 59x cross sections, and metallographic analysis) supported the conclusion that failure was due to applied stresses sufficient to fracture the castings which exhibited brittle overload cracks at highly stressed locations. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001200
EISBN: 978-1-62708-221-1
Abstract
During the operation of tractors with cantilevered body, the lateral wall of the hypoeutectic cast iron cylinder blocks cracked repeatedly. Three of the blocks were examined. The grain structure of the thick-walled part consisted of uniformly distributed graphite of medium flake size in a basic mass of pearlite with little ferrite. But the thin-walled part showed a structure of dendrites of precipitated primary solid solution grains with pearlitic-ferritic structure and a residual liquid phase with granular graphite in the ferritic matrix. The structure was formed by undercooling of the residual melt. In this case, it was promoted by fast cooling of the thin wall and had comparatively low strength. The fracture formation in the cylinder blocks was ascribed primarily to casting stresses. They could be alleviated by better filleting of the transition cross sections. The fracture was promoted by the formation of undercooled microstructure of low strength in the thin-walled part. Similar damage appeared in a cylinder head, in which case, the cracks were promoted by a supercooled structure.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001198
EISBN: 978-1-62708-221-1
Abstract
Cast iron bearing caps in tractor engines fractured repeatedly after only short operating periods. The fracture originated in a cast-in groove and ran approximately radially to the shaft axis. The smallest cross section was at the point of fracture. The core structure of the caps consisted of graphite in pearlitic-ferritic matrix. Casting stresses did not play a decisive role because of the simple shape of the pieces that were without substantial cross sectional variations. Two factors exerted an unfavorable effect in addition to comparatively low strength. First, the operating stress was raised locally by the sharp-edged groove, and second, the fracture resistance of the cast iron was lowered at this critical point by the existence of a ferritic bright border. To avoid such damage in the future it was recommended to observe one or more of the following precautions: 1) Eliminate the grooves; 2) Remove the ferritic bright border; 3) Avoid undercooling in the mold and therefore the formation of granular graphite; 4) Inoculate with finely powdered ferrosilicon into the melt for the same purpose; and, 5) Anneal at lower temperature or eliminate subsequent treatment in consideration of the uncomplicated shape of the castings.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c9001532
EISBN: 978-1-62708-232-7
Abstract
Work rolls made of indefinite chill double-poured (ICDP) iron are commonly used in the finishing trains of hot-strip mills (HSMs). In actual service, spalling, apart from other surface degeneration modes, constitutes a major mechanism of premature roll failures. Although spalling can be a culmination of roll material quality and/or mill abuse, the microstructure of a broken roll can often unveil intrinsic inadequacies in roll material quality that possibly accentuate failure. This is particularly relevant in circumstances when rolls, despite operation under similar mill environment, exhibit variations in roll life. The paper provides an insight into the microstructural characteristics of spalled ICED HSM work rolls, which underwent failure under similar mill operating environment in an integrated steel plant under the Steel Authority of India Limited. Microstructural features influencing ICDP roll quality, viz. characteristics of graphite, carbides, martensite, etc., have been extensively studied through optical microscopy, quantitative image analysis (QIA), and electron-probe microanalysis (EPMA). These are discussed in the context of spalling propensity and roll life.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0089617
EISBN: 978-1-62708-232-7
Abstract
A forged 4130 steel cylindrical permanent mold, used for centrifugal casting of gray- and ductile-iron pipe, was examined after pulling of the pipe became increasingly difficult. In operation, the mold rotated at a predetermined speed in a centrifugal casting machine while the molten metal, flowing through a trough, was poured into the mold beginning at the bell end and ending with the spigot end being poured last. After the pipe had cooled, it was pulled out from the bell end of the mold, and the procedure was repeated. Investigation supported the conclusion that failure of the mold surface was the result of localized overheating caused by splashing of molten metal on the bore surface near the spigot end. In addition, the mold-wash compound (a bentonite mixture) near the spigot end was too thin to provide the proper degree of insulation and to prevent molten metal from sticking to the bore surface. Recommendations included reducing the pouring temperatures of the molten metal and spraying a thicker insulating coating onto the mold surface.
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