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Weld cracks
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Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006819
EISBN: 978-1-62708-329-4
Abstract
This article offers an overview of fatigue fundamentals, common fatigue terminology, and examples of damage morphology. It presents a summary of relevant engineering mechanics, cyclic plasticity principles, and perspective on the modern design by analysis (DBA) techniques. The article reviews fatigue assessment methods incorporated in international design and post construction codes and standards, with special emphasis on evaluating welds. Specifically, the stress-life approach, the strain-life approach, and the fracture mechanics (crack growth) approach are described. An overview of high-cycle welded fatigue methods, cycle-counting techniques, and a discussion on ratcheting are also offered. A historical synopsis of fatigue technology advancements and commentary on component design and fabrication strategies to mitigate fatigue damage and improve damage tolerance are provided. Finally, the article presents practical fatigue assessment case studies of in-service equipment (pressure vessels) that employ DBA methods.
Series: ASM Handbook
Volume: 11A
Publisher: ASM International
Published: 30 August 2021
DOI: 10.31399/asm.hb.v11A.a0006808
EISBN: 978-1-62708-329-4
Abstract
This article describes some of the welding discontinuities and flaws characterized by nondestructive examinations. It focuses on nondestructive inspection methods used in the welding industry. The sources of weld discontinuities and defects as they relate to service failures or rejection in new construction inspection are also discussed. The article discusses the types of base metal cracks and metallurgical weld cracking. The article discusses the processes involved in the analysis of in-service weld failures. It briefly reviews the general types of process-related discontinuities of arc welds. Mechanical and environmental failure origins related to other types of welding processes are also described. The article explains the cause and effects of process-related discontinuities including weld porosity, inclusions, incomplete fusion, and incomplete penetration. Different fitness-for-service assessment methodologies for calculating allowable or critical flaw sizes are also discussed.
Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001777
EISBN: 978-1-62708-241-9
Abstract
The structural collapse of an iron-ore bucket-wheel stacker reclaimer at the beginning of operation was investigated by means of mechanical tests, microstructural characterization, and computational structural analysis. The mechanical failure was a consequence of a brittle fracture by cleavage. The crack followed the heat-affected zone of a welded joint connecting a rectangular hollow section member and a plate flange. The main factors contributing to failure were related with a combination of design-in and manufacturing-in factors like high load-strength ratio at the point of failure, local stress concentration as a result of geometry restrictions, and weld defects. This particular section was responsible for the load transfer between the front tie member and the boom extremity, and its failure was the main cause of the catastrophic failure of the equipment.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001186
EISBN: 978-1-62708-234-1
Abstract
A 2.3 mm diam steel wire broke during cable twisting. The fracture occurred obliquely to the longitudinal axis of the wire and showed a constriction at the end. Therefore it was a ductile fracture. File mark type work defects were noticeable on the wire surface at both sides of the fracture, but they had no effect on the breakage of the wire. Away from the fracture area, the wire had a normal structure of hyperfine lamellar pearlite (sorbite) of a “patented” and cold drawn steel wire. In the vicinity of the fracture, the cementite of the pearlite was partially spheroidized, while at the fracture itself it was completely spheroidized. Therefore the wire was locally annealed at this point. It was likely that the wire cracked at this point during the last drawing and then broke during twisting due to its lower strength in the weakened cross section after prior deformation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.petrol.c9001235
EISBN: 978-1-62708-228-0
Abstract
A welded natural gas line of 400 mm OD and 9 mm wall thickness made of unalloyed steel with 0.22C had to be removed from service after four months because of a pipe burst. Metallographic examination showed the pipe section located next to the gas entrance was permeated by cracks or blisters almost over its entire perimeter in agreement with the ultrasonic test results. Only the weld seam and a strip on each side of it were crack-free. Based on this investigation, the pipeline was taken out of service and reconstructed. To avoid such failures in the future, two preventative measures may be considered. One is to desulfurize the gas. Based on tests, however, the desulfurization would have to be carried very far to be successful. The second possibility is to dry the gas to such an extent as to prevent condensate, and this corrosion, from forming no matter how low winter temperatures may drop. This measure was ultimately recommended, deemed more effective and cheaper.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0047529
EISBN: 978-1-62708-230-3
Abstract
A weld that attached the head to the shell of a preheater containing steam at 1.4 MPa (200 psi) and was used in the manufacture of paper cracked in service. The original joint contained a 6.4 by 50 mm backing ring that had been tack welded to the inside surface of the shell in a position to project beyond the fully beveled top edge of the shell. The projecting edge of the ring fitted against a deep undercut on the inner corner of the rim of the head. The internal 90-deg angle in this undercut was sharp, with almost no fillet. A bevel from the lower edge of the undercut to the outside of the head completed the groove for the circumferential attachment weld. Investigation (visual inspection and actual size views etched in hot 50% hydrochloric acid) supported the conclusion that cracking occurred in the HAZ in the head of the original design, originating in the sharp corner of the undercut, which was an inherent stress raiser. Recommendations included revised joint design to ensure full root penetration.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001482
EISBN: 978-1-62708-229-7
Abstract
Penetration by molten copper occurred in the economizer of a large water-tube boiler. A cross section through a weld and the crack in the tube revealed a crack was an intergranular fissure. Small fissures of the same type also extended from its flanks. The main fissure was filled with an oxide scale in which were embedded particles having the appearance of metallic copper. It was concluded that the cracking that occurred at the time of re-welding was due to intergranular penetration by copper present in the deposit within the tubes, which had not been completely removed prior to welding. Subsequently, it was ascertained that trouble had been experienced with the centrifugal feed pumps, resulting in scuffing of some bronze rings. The presumption is that bronze particles had been carried in mechanical suspension in the feed water and deposited in the economizer tubes.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0048835
EISBN: 978-1-62708-220-4
Abstract
Welds in two CMo steel catalytic gas-oil desulfurizer reactors cracked under hydrogen pressure-temperature conditions that would not have been predicted by the June 1977 revision of the Nelson Curve for that material. Evidence of severe cracking was found in five weld-joint areas during examination of a naphtha desulfurizer by ultrasonic shear wave techniques. Defect indications were found in longitudinal and circumferential seam welds of the ASTM A204, grade A, steel sheet. The vessel was found to have a type 405 stainless steel liner for corrosion protection that was spot welded to the base metal and all vessel welds were found to be overlaid with type 309 stainless steel. Long longitudinal cracks in the weld metal, as well as transverse cracks were exposed after the weld overlay was ground off. A decarburized region on either side of the crack was revealed by metallurgical examination of a cross section of a longitudinal crack. It was concluded that the damage was caused by a form of hydrogen attack. Installation of a used Cr-Mo steel vessel with a type 347 stainless steel weld overlay was suggested as a corrective action.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001570
EISBN: 978-1-62708-220-4
Abstract
Corrosion failure occurred in a titanium clad tubesheet because of a corrosive tube-side gas-liquid mixture leaking through fatigue cracks in the seal welds at tube-to-tubesheet joints. The tubesheet was a carbon steel plate clad with titanium on the tube side face. The seal weld cracks were initiated by cyclic stress imposed by exchanger tubes. The gas-liquid mixture passed through cracks under tube-side pressure, resulting in severe corrosion of the steel backing plate. The failure started with the loosening of the expanded tube-to-tubesheet joints. Loose joints allowed the exchanger tubes to impose load on seal welds and the shell side cooling water entered the crevice between the tubesheet and the tubes. The cooling water in the crevice caused galvanic reaction and embrittlement of seal welds. Brittle crack opening and crack propagation in seal welds occurred due to the cyclic stress imposed by the tubes. The cyclic stress arised from the thermal cycling of the heat exchanger. The possible effects of material properties on the failure of the tubesheet are discussed.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0091009
EISBN: 978-1-62708-235-8
Abstract
A thick-walled tube that was weld fabricated for use as a pressure vessel exhibited cracks. Similar cracking was apparent at the weld toes after postweld stress relief or quench-and-temper heat treatment. The cracks were not detectable by nondestructive examination after welding, immediately prior to heat treatment. Multiple-pass arc welds secured the carbon-steel flanges to the Ni-Cr-Mo-V alloy steel tubes. Investigation (visual inspection, metallographic analysis, and evaluation of the fabrication history and the analysis data) supported the conclusion that the tube failed as a result of stress-relief cracking. Very high residual stresses often result from welding thick sections of hardenable steels, even when preheating is employed. Quenched-and-tempered steels containing vanadium, as well as HSLA steels with a vanadium addition, have been shown to be susceptible to this embrittlement. Manufacturers of susceptible steels recommend use of these materials in the as-welded condition.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0091048
EISBN: 978-1-62708-235-8
Abstract
A welded ferritic stainless steel heat exchanger cracked prior to service. The welding filler metal was identified as an austenitic stainless steel and the joining method as gas tungsten arc welding. Investigation (visual inspection, SEM images, 5.9x images, and 8.9x/119x images etched with Vilella's reagent followed by electrolytic etching in 10% oxalic acid) supported the conclusion that the heat exchanger cracked due to weld cold cracking or postwelding brittle overload that occurred via flexure during fabrication. The brittle nature of the weld was likely due to a combination of high residual stresses, a mixed microstructure, inclusions, and gross grain coarsening. These synergistic factors resulted from extreme heat input during fillet welding. Recommendations included altering the welding variables such as current, voltage, and travel speed to substantially reduce the heat input.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0089738
EISBN: 978-1-62708-235-8
Abstract
While undergoing vibration testing, a type 347 stainless steel inlet header for a fuel-to-air heat exchanger cracked in the header tube adjacent to the weld bead between the tube and header duct. Investigation (visual inspection and liquid penetrant inspection) supported the conclusion that the crack in the header tube was the result of a stress concentration at the toe of the weld joining a doubler collar to the tube. The stress concentration was caused by undercutting from poor welding technique and an unfavorable joint design that did not permit a good fit-up. Recommendations included manufacturing the doubler collar so that it could be placed in intimate contact with the header duct, and a revised weld procedure was recommended to result in a smaller, controlled, homogeneous weld joint with less distortion.
Series: ASM Failure Analysis Case Histories
Volume: 2
Publisher: ASM International
Published: 01 December 1993
DOI: 10.31399/asm.fach.v02.c9001322
EISBN: 978-1-62708-215-0
Abstract
A failed SAE-192 carbon steel tube from a 6.2-MPa (900-psig), 200-Mg/h (180-ton/h) capacity refinery boiler was analyzed to determine its failure mode. Optical and SEM examination results were combined with knowledge of the boiler operating conditions to conclude that the failure was hydrogen-induced. The hydrogen was probably generated by the steam-iron reaction. The source of steam on the flue gas side could be traced to a cracked fillet weld in the boiler The failure mode was unusual in that the attack was found to originate from the flue gas side of the tube rather than the steam side.