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1-6 of 6
Lamellar tearing
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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001442
EISBN: 978-1-62708-221-1
Abstract
The impeller of a 4 ft. diam extraction fan driven by a 120 hp motor at 1,480 rpm. disrupted suddenly. The majority of the vanes had become detached where they were welded to the plates. At other locations, separation of the vanes was accompanied by tearing of the adjacent plate, failure being initiated at the weld fillets of the inner end of the vanes. An unusual feature was that the blades disclosed regions having a pronounced striated and stepped appearance. The etched microstructure was typical of a low carbon rolled plate having the usual banded appearance. A cross section through the fillet welds and zone showed lamellar tearing, which confirmed that failure had occurred in weld metal adjacent to the fusion face of the fillet to the vane. Results of the investigation indicated that the primary cause of failure of the impeller was the development of fatigue cracks from the unwelded roots of the fillet welds, by which the vanes were attached to the supporting plates. The impeller would have shown increased resistance to fatigue crack initiation if the T joint between the vanes and plates had been of the full penetration type.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.conag.c9001139
EISBN: 978-1-62708-221-1
Abstract
A truck-mounted hydraulic crane had a horizontal thrust bearing with one race attached to the truck and the other to the rotating crane. The outside race of the bearing was driven by a pinion gear, and it is through this mechanism that the crane body rotated about a vertical axis. The manufacturer welded the inner race to the carrier in a single pass. After several years of service, the attachment weld between the bearing inner race and the turntable failed in the area adjacent to the heat-affected zone. The fracture zone where there was the greatest tension was heavily oxidized. In the zone where the bearing was in compression, there was a clean surface indicating recent fracture. Finally, there were areas where the weld did not meet AWS specifications for convexity or concavity. These areas were weak enough to allow fatigue cracks to initiate. Recommendations to prevent reoccurrence of the failure include the use of bolts in lieu of welding, a welding schedule that reduces the propensity of lamellar tearing, and the use of an alloy that precludes lamellar tearing. However, if abuse of the crane was the primary cause of failure, none of these recommendations would have prevented deterioration of the machine to an extent that would have rendered the failure improbable.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001141
EISBN: 978-1-62708-227-3
Abstract
During a refit of a twenty-year-old Naval destroyer, two cracks were found on the inside of the killed carbon-manganese steel hull plate at the forward end of the boiler room. The cracks coincided with the location of the top and bottom plates of the bilge keel. Metallurgical examination of sections cut from the cracked area identified lamellar tearing as the principle cause of the cracking. This was surprising in 6 mm thick hull plates. Corrosion fatigue and general corrosion also contributed to hull plate perforation. Although it is probable that more lamellar tears exist near the bilge keel in other ships and may be a nuisance in the future, the hull integrity of the ships is not threatened and major repairs are not needed.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0089793
EISBN: 978-1-62708-235-8
Abstract
During the final shop welding of a large armature for a direct-current motor (4475 kW, or 6000 hp), a loud bang was heard, and the welding operation stopped. When the weld was cold, nondestructive evaluation revealed a large crack adjacent to the root weld. Investigation showed the main crack had propagated parallel to the fusion boundary along the subcritical HAZ and was associated with long stringers of type II manganese sulfide (MnS) inclusions. This supported the conclusion that the weld failed by lamellar tearing as a result of the high rotational strain induced at the root of the weld caused by the weld design, weld sequence, and thermal effects. Recommendations included removing the old weldment to a depth beyond the crack and replacing this with a softer weld metal layer before making the main weld onto the softer layer.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001446
EISBN: 978-1-62708-234-1
Abstract
A 2 ft. diam 20 ft. long cylinder with a wall thickness of 1 in. used for the transportation of a compressed gas failed by cracking. The cylinder was forged in a low ally steel. The working pressure was 3000 psi and it had been in service for about seven years. A longitudinal crack, about 2 in. long, developed at the approximate mid-length of the vessel, and allowed slow de-pressurization. Subsequent examination by radiography and ultrasonic means indicated the crack was associated with an irregularly shaped, laminar type of defect located within the wall of the vessel. It was concluded that failure of this vessel resulted from the development of a radial crack orientated in the axial direction. This appeared to have originated on the bore surface in a region where the laminar defect closely approached this surface. The defect was introduced during the manufacture of the vessel, probably originating as a secondary pipe in the ingot which was subsequently displaced and forced into the wall of the vessel during the piercing operation.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0048840
EISBN: 978-1-62708-220-4
Abstract
A spherical carbon steel fixed-catalyst bed reactor, fabricated from French steel A42C-3S, approximately equivalent to ASTM A201 grade B, failed after 20 years of service while in a standby condition. The unit was found to contain primarily hydrogen at the time of failure. The vessel had a type 304 stainless steel shroud around the catalyst bed as protection against the overheating that was possible if the gas bypassed the bed through the refractory material. The failure was observed to have begun at the toe of the shroud-support ring weld. The ring was found to have a number of small cracks at the root of the weld. The cleavage mode of fracture was confirmed by SEM. The presence of extensive secondary cracking and twinning (Neumann bands) where the fracture followed the line of the shroud-support ring was revealed by metallography. It was revealed by refinery maintenance records that the ring had been removed for hydrotest and welded without any postweld heat treatment. The final cause of failure was concluded to be cracking that developed during the installation of the new shroud ring. Stress-relief heat treatments were recommended to be performed to reduce residual-stress levels after welding.