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Exfoliation corrosion
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0048299
EISBN: 978-1-62708-229-7
Abstract
Pendant-style reheater, constructed of ASME SA-213, grade T-11, steel ruptured. A set of four tubes, specified to be 64 mm OD x 3.4 mm minimum wall thickness was examined. A small quantity of loose debris was removed from the inside of one of the tubes. The major constituent was revealed by EDS analysis of the debris to be iron with traces of phosphorus, manganese, sodium, calcium, copper, zinc, potassium, silicon, chromium, and molybdenum. Thus the debris was interpreted to be the scale from ID of the tube with boiler feedwater chemicals from the attemperation spray. The likely cause of failure was concluded to be exfoliation of the scale from the ID surface of the tube. Creep failures were interpreted to be caused by localized temperatures higher than the maximum service temperature. Replacement of the affected tubes was recommended. Inspection of the tubes by radiography to find the circuits with the greatest accumulation of debris and replacing them as necessary was recommended on an annual basis.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001710
EISBN: 978-1-62708-229-7
Abstract
Aluminum-clad spent nuclear fuel is stored in water filled basins at the Savannah River Site awaiting processing or other disposition. After more than 35 years of service underwater, the aluminum storage racks that position the fuel bundles in the basin were replaced. During the removal of the racks from the basin, a failure occurred in one of the racks and the Savannah River Technology Center was asked to investigate. This paper presents the results of the failure analysis and provides a discussion of the effects of corrosion on the structural integrity of the storage racks.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0047199
EISBN: 978-1-62708-234-1
Abstract
The lower receiver of the M16 rifle is an anodized forging of aluminum alloy 7075-T6. Degradation of the receivers was observed after three years of service in a hot, humid atmosphere. The affected areas were those in frequent contact with the user's hands. There was no question that the material failed as a result of exfoliation corrosion, so an investigation was undertaken, centered around the study of thermal treatments that would increase the exfoliation resistance and still develop the required 448 MPa (65 ksi) yield strength. The results of the study concluded that rolled bar stock should be preferred to extruded bar stock. Differences in grain structure of the forgings, as induced by differences in thermal-mechanical history of the forged material, can have a significant effect on susceptibility to exfoliation corrosion. Regarding thermal treatment, the results show conclusively that large changes in strength and exfoliation characteristics of 7075 forgings can be induced by changes in temperature or time of thermal treatment. With regard to the effect of quenching rate on exfoliation characteristics, a cold-water quench below 25 deg C (75 deg F) would appear to be far superior to an elevated-temperature quench to minimize exfoliation for 7075 forgings in the T6 temper.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001455
EISBN: 978-1-62708-234-1
Abstract
Aluminum alloy BS.1476-HE.15 by virtue of its high strength and low density finds application in the form of bars or sections for cranes, bridges, and other such structures where a reduction in dead weight load and inertia stresses is advantageous. Bars and sections in H.15 alloy are mostly produced by extrusion. Some material processed this way has been prone to exfoliation corrosion. Extended aging for 24 h at a temperature of 185 deg C (365 deg F) virtually suppresses the tendency for exfoliation corrosion to develop. Also, the use of a sprayed coating, either of aluminum or Al-1Zn alloy, was effective in halting and preventing this form of attack. While alarming, the appearance of exfoliation corrosion provides a valuable warning to the engineer or inspector before a severe weakening of the particular sections has occurred.