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Series: ASM Failure Analysis Case Histories
Volume: 3
Publisher: ASM International
Published: 01 December 2019
DOI: 10.31399/asm.fach.v03.c9001833
EISBN: 978-1-62708-241-9
Abstract
The failure of a boiler operating at 540 °C and 9.4 MPa was investigated by examining material samples from the near-failure region and by thermodynamic analysis. A scanning Auger microprobe, SEM, and commercial thermodynamic software codes were used in the investigation. Results indicated that the boiler failure was caused by grain-boundary segregation of phosphorous, tin, and nitrogen and the in-service formation of carbide films and granules on the grain boundaries.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001736
EISBN: 978-1-62708-220-4
Abstract
Leakage was detected at the welds between stiffening plates and the pipe in a transfer line carrying butane and related petrochemical compounds. The line and reinforcing rings were of AISI 316 stainless steel, the pipe being of 508 mm diam and 6.25 mm wall thickness. The design temperature and pressure were 621 deg C and 2.75 kPa, respectively, while the operating conditions were 579 deg C and 1.03 kPa. The line was insulated. Failure occurred after approximately 90,000 h of operation, shutdowns being approximately two per annum. The cracking occurred at the toe of welds between the plates and the pipe. The creep damage failure was attributed to repeated relaxation cycles of very high thermal stresses of resulting from the periodic shutdowns, temperature fluctuations during service, or both. This failure emphasized the information available from an evaluation of the operative creep mechanism, namely grain boundary sliding, relating to the periodic nature of the loading, with high residual stresses being present.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001687
EISBN: 978-1-62708-220-4
Abstract
Microstructural examinations on transverse cross sections of a steam reformer tube, showed the presence of large macrovoids elongated in the radial direction and emanating from the internal surface of the tube. The macrovoids were located at the interdendritic regions, and were partially filled by a Mn-Fe bearing chromium oxide film. The areas adjacent to the oxide film were chemically depleted in C, Cr and Mn and rich in Fe and Ni. Associated with this depletion were a large concentration of microvoids. It was suggested that the dissolution of carbides in areas surrounding the macrovoids and the concentration of stresses at their tips, caused extensive localized plastic deformation which led to the formation of microvoids and subsequently to the spalling of the oxide film. The non-protective character of the film induced a progressive deterioration of the grain boundaries properties. Grain boundary sliding and dislocation motion were enhanced, causing a local increase in the steady state strain rate and the premature failure of the tube.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0048309
EISBN: 978-1-62708-229-7
Abstract
A 75 mm OD x 7.4 mm wall thickness carbon steel boiler tube ruptured. A substantial degree of corrosion on the water-side surface leaving a rough area in the immediate vicinity of the rupture was revealed by visual examination. Decarburization and extensive discontinuous intergranular cracking was revealed by microscopic examination of a cross section through the tube wall at the fracture. It was concluded that the rupture occurred because of hydrogen damage involving the formation of methane by the reaction of dissolved hydrogen with carbon in the steel. Hydrogen was produced by the chemical reaction that corroded the internal tube surface. Steel embrittled by hydrogen can be restored only if grain boundary cracking or decarburization had not occurred but since the material embrittled in this manner, its replacement was recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001004
EISBN: 978-1-62708-229-7
Abstract
The results of a failure analysis of a series of Cr-Mo-V steel turbine studs which had experienced a service lifetime of some 50,000 h are described. It was observed that certain studs suffered complete fracture while others showed significant defects located at the first stress bearing thread. Crack extension was the result of marked creep embrittlement and reverse temper embrittlement (RTE). Selected approaches were examined to assess the effects of RTE on the material toughness of selected studs. It was observed that Auger electron microscopy results which indicated the extent of grain boundary phosphorus segregation exhibited a good relationship with ambient temperature Charpy data. The electrochemical polarization kinetic reactivation, EPR, approach, however, proved disappointing in that the overlapping scatter in the minimum current density, Ir, for an embrittled and a non-embrittled material was such that no clear decision of the toughness properties was possible by this approach. The initial results obtained from small punch testing showed good agreement with other reported data and could be related to the FATT. Indeed, this small punch test, combined with a miniature sample sampling method, represents an attractive approach to the toughness assessment of critical power plant components.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0090114
EISBN: 978-1-62708-229-7
Abstract
The first-stage blades in a model 501D5 gas turbine had 16 cooling holes. After 32,000 h of service, the blades exhibited cracking at the cooling holes. The blade material was wrought Udimet 520 alloy, with nominal composition of 57Ni-19Cr-12Co-6Mo-1W-2Al-3Ti-0.05C-0.005B. The cooling holes' surface was not coated. Investigation supported the conclusions that the cracking at the cooling holes was due to grain-boundary oxidation and nitridation at the cooling hole surface, embrittlement and loss of local ductility of the base alloy, temperature gradient from the airfoil surface to the cooling holes, which led to relatively high thermal stresses at the holes located at the thicker sections of the airfoil, and stress concentration of 2.5 at the cooling hole and the presence of relatively high total strain (an inelastic strain of 1.2%) at the cooling hole surface. Recommendations include applying the specially designed methods given in this case study to estimate the metal temperature and stresses in order to predict the life of turbine blades under similar operating conditions.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c0091756
EISBN: 978-1-62708-236-5
Abstract
An alloy IN-690 (N06690) incinerator liner approximately 0.8 mm (0.031 in.) thick failed after only 250 h of service burning solid waste. Investigation supported the conclusion that the root cause of the failure was overfiring during startup and sulfidation of the nickel-base alloy. No recommendations were made.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0045918
EISBN: 978-1-62708-235-8
Abstract
Cracks, with no other damage, were observed in a niobium alloy (Nb-106) part when it was pulled from several months of protective storage for assembly into a rocket nozzle. SEM views showed the cracks to be intergranular, with contaminant particles on a large number of the grain facets. EDX analysis showed they consisted of niobium and fluorine. Plastic replicas, prepared by standard TEM techniques, were analyzed with selected-area electron diffraction, showing a pattern match for niobium tetrafluoride. Auger analyses showed electron spectra containing peaks representing carbon, oxygen, nitrogen, fluorine, and chlorine. Investigation into the processing history of the part showed the tenacious oxide film formed by the affinity of niobium for oxygen - even when heat treated in a vacuum – was removed with a combination of strong acids: nitric, hydrochloric, hydrofluoric, and lactic, resulting in the contaminants found on the surface. Thus, residues of the cleaning acid on the part had caused SCC during storage, with the tensile stresses necessary to generate SCC assumed to have been residual stresses from the heat treatment. Recommendation was made that more stringent cleaning procedures to remove any trace of the cleaning acids be used.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047756
EISBN: 978-1-62708-235-8
Abstract
Waspaloy (AMS 5586) fabricated inner ring of a spray-manifold assembly failed transversely through the manifold tubing at the edge of the tube and support sleeve brazed joint. The assembly was brazed with AWS BAu-4 filler metal (AMS 4787). Fatigue beach marks propagating from extremities of a granular gold-tinted surface region adjacent to the tube-to-sleeve brazed joint and extending circumferentially were revealed by microscopic examination. Embrittlement of the tube caused by molten braze metal penetration along grain boundaries was evidenced by micrographs of a granular portion of the fracture. It was revealed by the initial fracture profile that fatigue cracks begun as an intergranular separation and subsequently became transgranular. It was concluded that failure of the tube was caused by excessive alloying between the braze metal and the Waspaloy. Reduced temperatures during torch debrazing or rebrazing were recommended to minimize molten braze metal penetration.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047602
EISBN: 978-1-62708-235-8
Abstract
Parts of 21Cr-6Ni-9Mn stainless steel that had been forged at about 815 deg C (1500 deg F) were gas tungsten arc welded. During postweld inspection, cracks were found in the HAZs of the welds. Welding had been done using a copper fixture that contacted the steel in the area of the HAZ on each side of the weld but did not extend under the tungsten arc. In SEM examination, the cracks appeared to be intergranular and extended to a depth of approximately 1.3 mm (0.05 in.). The crack appearance suggested that the surface temperature of the HAZ could have melted a film of copper on the fixture surface and that this could have penetrated the stainless steel in the presence of tensile thermal-contraction stresses. The cracks in the weldments were a form of liquid-metal embrittlement caused by contact with superficially melted copper from the fixture and subsequent grain-boundary attack of the stainless steel in an area under residual tensile stress. The copper for the fixtures was replaced by aluminum. No further cracking was encountered.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047632
EISBN: 978-1-62708-235-8
Abstract
An air bottle, machined from a solid block of aluminum alloy 2219-T852, displayed liquid-penetrant crack indications after assembly welding. The air bottle was machined to rough shape, a 3.8 mm (0.15 in.) wall thickness cylindrical cup with a 19 mm (3/4 in.) wall thickness integral boss on one side. After annealing, hot spinning, annealing a second time, and tack welding a port fitting, the assembly was torch preheated to 120 to 150 deg C (250 to 300 deg F). The port fitting was then welded in place. Final full heat treatment to the T62 temper was followed by machining, testing, and inspection. The crack indications were found only on one side of the boss and on the lower portion of the hot-spun dome region. The metallographic specimens revealed triangular voids and severe intergranular cracks. The cracks displayed the glossy surfaces typical of melted and resolidified material. The localized cracks in the air bottle were from grain-boundary eutectic melting caused by local torch overheating used in preparation for assembly welding of a port fitting. A change in design was scheduled to semiautomatic welding without the use of preheating for the joining of the port fitting for the dome opening.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001217
EISBN: 978-1-62708-235-8
Abstract
In a housing made of cast steel GS 20MoV12 3, weighing 42 tons, precipitates were found on the austenitic grain boundaries during metallographic inspection. According to their shape and type they were recognized as carbides that precipitated during tempering. In addition, a much coarser network of rod-shaped and plate-shaped precipitates was found, that probably corresponded to the primary grain boundaries, or to the grain boundaries or twin planes of the austenite formed during solidification of the melt. These particles could have been aluminum nitride judging by their shape and order of precipitation. Tests showed that a subsequent removal of this defect by solutioning was impractical because the annealing temperature was too high. To avoid this defect in the future the sole recommendation is to accelerate the cooling rate through the critical region between 1200 to 900 deg C to such an extent as is practicable with respect to machinability.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048399
EISBN: 978-1-62708-226-6
Abstract
Two of four adjustable Moore pins, which had been used to stabilize a proximal femur fracture, were found to be broken and deformed at their threads. The pins were made from a cobalt-chromium alloy and were not in the same condition. Brittle precipitates in the grains and grain boundaries were seen in one of the pins and hence the fracture was revealed to have occurred along the grain boundaries. The other pin made from cold-worked cobalt-chromium alloy was observed to have randomly lines of primary inclusions. Intermingled dimples and fatigue striations were exhibited on the fracture surface of this pin. Thus, the effect of different conditions of cobalt-chromium alloys on failure behavior was demonstrated as a result of this study.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001223
EISBN: 978-1-62708-233-4
Abstract
The corner of a welded sheet construction made from austenitic corrosion-resistant chromium-nickel steel showed corrosive attack of the outer sheet. This attack was most severe at the points subjected to the greatest heat during welding. Particularly large amounts of weld metal had been applied. Microscopic examination showed grain disintegration was promoted by the thickness of the weld bead and the amount of heat required to produce it. If nonstabilized austenitic sheet is to be used in the future, one of the particularly low-carbon steels, X2 CrNi 18 9 or X2 CrNiMo 18 10, is recommended.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.steel.c0046956
EISBN: 978-1-62708-232-7
Abstract
A brazing-furnace muffle 34 cm (13 in.) wide, 26 cm (10 in.) high, and 198 cm (78 in.) long, was fabricated from nickel-base high-temperature alloy sheet and installed in a gas-fired furnace used for copper brazing of various assemblies. The operating temperature of the muffle was reported to have been closely controlled at the normal temperature of 1175 deg C (2150 deg F); a hydrogen atmosphere was used during brazing. After about five months of continuous operation, four or five holes developed on the floor of the muffle, and the muffle was removed from service. Analysis (visual inspection, x-ray spectrometry, and metallographic examination) supported the conclusion that the muffle failed by localized overheating in some areas to temperatures exceeding 1260 deg C (2300 deg F). The copper found near the holes had dripped to the floor from assemblies during brazing. The copper diffused into the nickel-base alloy and formed a grain-boundary phase that was molten at the operating temperature. The presence of this phase caused localized liquefaction and weakened the alloy sufficiently to allow formation of the holes. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001681
EISBN: 978-1-62708-234-1
Abstract
A microstructural analysis has been made of a burner nozzle removed from service in a coal gasification plant. The nozzle was a casting of a Co-29wt%Cr-19wt%Fe alloy. Extensive hot corrosion had occurred on the surface. There was penetration along grain boundaries, and corrosion products in these regions were particularly rich in S, and also contained Al, Si, O, and Cl. The grain boundaries contained Cr-rich particles which were probably Cr23-C6 type carbides. In the matrix, corrosion occurred between the Widmanstatten plates. Particles were found between these plates, most of which were rich in Cr and O, and probably were Cr2-O3 oxides. Other matrix particles were found which were rich in Al, O, and S. The corrosion was related to these grain boundary and matrix particles, which either produced a Cr-depleted zone around them or were themselves attacked.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c9001734
EISBN: 978-1-62708-234-1
Abstract
An aircraft engine in which an in-flight fire had occurred was dismantled and examined. A bracket assembly fabricated from 2024 aluminum, one of several failed components, was of prime interest because of apparent heat damage. Scanning electron microscopy was used to compare laboratory-induced fractures made at room and elevated temperatures with the bracket failure. The service failure exhibited grain separation and loss of delineation of the grain boundaries due to melting. SEM revealed deep voids between grains and tendrils that connected grains, which resulted from surface tension during melting. Microscopic examination of polished, etched section through the fractured surface verified intergranular separation and breakdown of grain facets. The absence of any reduction of thickness on the bracket assembly at the point of fracture, along with evidence of intense heat at this point, indicated that little stress had been applied to the part. Comparisons of the service failure and laboratory-induced failures in conjunction with macroscopic and metallographic observations showed that the bracket assembly failed because an intense, localized flame had melted the material.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.machtools.c9001574
EISBN: 978-1-62708-223-5
Abstract
A CrN coated restrike punch was made of WR-95 (similar to H-11), which was fluidized bed nitrided. The coated punch was used on hot Inconel at about 1040 deg C (1900 deg F). However, a water-soluble graphite coolant was used to maintain the punch temperature at 230 deg C (450 deg F). Visual and binocular inspection at 64+ revealed presence of cracks and complete washout of coating in the working area of the failed punch. Comparison of metallographic cross sections of used and unused punches revealed a significant microstructural transformation in case of the used punch. Presence of a yellow porous layer was clearly evident between the nitrided layer and the coating, in case of the used punch. Cracks were observed to propagate from the outer surface into the bulk. Oxidation was evident along the cracks. The microstructural transformation observed in the case of the used punch was a clear indication of high temperature exposure (due to insufficient cooling) during application. The most probable cause of failure was thermal fatigue.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.aero.c0006394
EISBN: 978-1-62708-217-4
Abstract
A preflight inspection found a broken diaphragm from a side controller fabricated from 17-7 PH stainless steel in the RH 950 heat treatment condition. Failure occurred by cracking of the base of the flange-like diaphragm. The crack traveled 360 deg around the diaphragm. Scanning electron microscopy (SEM) revealed that the failure occurred by a brittle intergranular mechanism and stress-corrosion cracking (SCC), and indicated a failure mode of selective grain-boundary separation. The diaphragms were heat treated in batches of 25. An improper heat treatment could have resulted in the formation of grain boundary precipitates, including chromium carbides. It was concluded that failure of the diaphragm was due to a combination of sensitization caused by improper heat treatment and subsequent SCC. It was recommended that the remaining 24 sensor diaphragms from the affected batch be removed from service. In addition, a sample from each heat treat batch should be submitted to the Strauss test (ASTM A262, practice E) to determine susceptibility to intergranular corrosion. Also, it was recommended that a stress analysis be performed on the system to determine whether a different heat treatment (which would offer lower strength but higher toughness) could be used for this part.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.homegoods.c9001694
EISBN: 978-1-62708-222-8
Abstract
The outer tube, or stem, on a bicycle frame fractured after two years of use. Detailed investigation revealed that the lower stem bearing had been loose for some time and the bottom bearing cup contained many cracks. Metallographic examination of the chromium-plated cup confirmed the brittle nature of the cracks, located along prior austenite boundaries. The failure was attributed to hydrogen embrittlement due to improper manufacturing procedures following chromium plating. The cracking led to looseness in the bearing and consequent scoring, cracking, and overloading of the stem.