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Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0090909
EISBN: 978-1-62708-235-8
Abstract
An injection-molded PVC water-filter housing fractured in service. 75x views and visual inspection supported the conclusion that failure occurred due to fatigue crack propagation, as indicated by the presence of discontinuous crack-growth bands and their evolution. However, an initial fissure was believed to have started first due to residual stresses developed during injection molding. No recommendations were made.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c9001400
EISBN: 978-1-62708-235-8
Abstract
Following the discovery numerous cracks at many of the welded seams of a mild steel CO2 absorber vessel, a sample for examination was removed from the worst affected area where repairs had been effected. A 12 in. long circumferential crack was visible. Specimens were taken to cover the several locations of cracking which, in all cases, were found to be similar and of the intergranular type filled with oxide or corrosion product. The association of the cracks with the weld seams indicated that contraction stresses from welding were primarily responsible. Failure of the absorber vessel was found to be due to stress corrosion. Although the active agent present was not positively identified, the aqueous solution of monoethanolamine was thought to be the most probable. The origin of the stresses was not elucidated but the association of the cracks with the welded seams indicated inherent residual stresses as being primarily responsible. Tests carried out tend to suggest that stress relief was not carried out. For the replacement plant, consideration of stress relieving or the use of an alternative material was advised.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001567
EISBN: 978-1-62708-230-3
Abstract
A falling film black liquor evaporator consisted of flat twin plate heat exchangers and was used to increase black liquor solids content prior to its burning in the recovery boiler. Several plate heat exchangers were fabricated of AISI type 316L stainless steel by electric resistance welding. Cracks initiated at the inside surface of the welded areas and penetrated through the wall thickness. In several locations, the weld fractured and the plates separated with significant spring back, indicative of high residual stresses attributed to fabrication and weld procedures. The cracks had extended radially from the electric resistant weld into the base metal. Metallographic examination revealed the cracks were transgranular and branching, characteristic of SCC in austenitic stainless steels. The fracture surfaces had a brittle cleavage-like appearance, typical of SCC in austenitic stainless steels. Chlorides in the service environment were a contributory factor. The primary factor causing SCC localized at the electric resistant welds was substantial residual stresses as a result of fabrication procedures. It was recommended that the heat exchanger plates be subjected to stress-relief heat treatment following fabrication and welding.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c0091699
EISBN: 978-1-62708-219-8
Abstract
Eddy-current inspection was performed on a leaking absorber bundle in an absorption air-conditioning unit. The inspection revealed crack-like indications in approximately 50% of the tubes. The tube material was phosphorus-deoxidized copper. Investigation (visual inspection, chemical analysis, 0.75x images, 2x macrographs after light acid cleaning to remove corrosion product, and 75x micrographs) supported the conclusion that the absorber tubes failed by SCC initiated by ammonia contamination in the lithium bromide solution. No recommendations were made.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.modes.c0090460
EISBN: 978-1-62708-234-1
Abstract
A component of a water filtration unit failed while being used in service for approximately eight months. The filter system had been installed in a commercial laboratory, where it was stated to have been used exclusively in conjunction with deionized water. The failed part had been injection molded from a 30% glass-fiber and mineral-reinforced nylon 12 resin. Investigation, including visual inspection, 118x SEM images, 9x micrographs, energy-dispersive x-ray spectroscopy, micro-FTIR in the ATR mode, and TGA, supported the conclusion that the filter component failed as a result of molecular degradation caused by the service conditions. Specifically, the part material had undergone severe chemical attack, including oxidation and hydrolysis, through contact with silver chloride. The source of the silver chloride was not established, but one potential source was photographic silver recovery.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0047611
EISBN: 978-1-62708-220-4
Abstract
Several tubes in a tube bundle in an evaporator used to concentrate an acid nitrate solution failed by leakage. The feed to the evaporator contained about 6% nitrate, and the discharge about 60% nitrate. The tube bundle was comprised of type 309S (Nb) stainless steel drawn-and-welded tubes expanded and welded into two type 304L stainless steel tube sheets. The tubes failed by crevice corrosion. The failed tubes were defective as-received, and the establishment of concentration cells within the longitudinal cracks in the seam welds led to ultimate corrosive penetration of the wall. There was no evidence of crevice corrosion or any localized penetration of tubes that had sound welds. The leaking type 309S (Nb) welded tubes should be replaced with seamless tubes of type 304L stainless steel to minimize the areas requiring welding and to provide maximum weldability for the tube-sheet joints.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001404
EISBN: 978-1-62708-220-4
Abstract
After about four years of service, cracks appeared on the internal or process-side surfaces of four evaporator pans in a sugar concentrator. The pans consisted of a Mo stabilized austenitic stainless steel inner vessel surrounded by a mild steel steam jacket. Corrosion of the external surface had taken place in the form of confluent pitting over a band adjacent to the fillet weld which attached the pan to the blocking ring. Numerous cracks were present in this corroded zone. Microscopical examination of several specimens cut from the sample revealed that the internal cracks in the pan itself originated from the external side of the plate, i.e. from the region covered by the shrouding ring. They were predominantly of the transgranular type. Because the cracks were not of the intergranular type as usually found with weld decay, they were considered to be indicative of stress-corrosion cracking. Stresses responsible for the cracking resulted from weld contraction. The pans had been hosed down periodically with water from local boreholes to remove sugar from the external surfaces, which introduced the corrosive medium.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0060104
EISBN: 978-1-62708-220-4
Abstract
Eddy current inspection was performed on a vertical evaporator unit (that contained 180 tubes) used in a chemical processing plant. It was advised that the tube material was type 316 stainless steel. The shell-side fluid was condensate and gaseous methylene chloride, while the tube-side fluid was contaminated liquid methylene chloride. More than 100 tubes exhibiting severe outer surface pitting and cracklike indications near each tube sheet were revealed during eddy current inspection. It was observed that the indications correlated with rust-stained, pitted, and cracked areas on the outer surfaces. The cracking was revealed by metallographic examination to have initiated from the outer surface, frequently at pits, and penetrated the tube wall in a transgranular, branching fashion. The crack features were characteristic of chloride stress-corrosion cracking. A change in tube material was recommended to avoid future failures and loss of service.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001067
EISBN: 978-1-62708-214-3
Abstract
The source of cracking in the circumferential weld seam in a JIS-SM50B carbon-manganese steel pipe used in a CO2 absorber was investigated, the absorber had been in service for 18 years. The seam had been weld-repaired twice, and the repair welds had been locally stress relieved. Longitudinal seams in the same vessel, which had been stress relieved in a furnace, showed no tendency toward cracking. The solution passing through the vessel contained CO2-CO-H20, KHCO, and Cl− ions. Nondestructive testing revealed that the cracks originated in the heat-affected zone and propagated into the base metal and weld. Severe branching of the cracks characteristic of stress-corrosion cracking was observed. Microexamination revealed that crack propagation was transgranular further supporting the possibility of stress-corrosion cracking. Simulation tests carried out in the vessel confirmed this mode of cracking. It was recommended that weld seams be furnace heat treated at a temperature of 600 to 640 deg C (1110 to 1180 deg F) for a minimum of 1 h per inch of section thickness.
Series: ASM Failure Analysis Case Histories
Volume: 1
Publisher: ASM International
Published: 01 December 1992
DOI: 10.31399/asm.fach.v01.c9001032
EISBN: 978-1-62708-214-3
Abstract
A Stirling engine heat pipe failed after only 2h of operation in a test situation. Cracking at the leading edge of an evaporator fin allowed air to enter the system and react with the sodium coolant. The fin was fabricated from 0.8 mm (0.03 in.) thick Inconel 600 sheet. The wick material was type 316 stainless steel. Macro- and microexaminations of specimens from the failed heat pipe were conducted. The fin cracking was caused by overheating that produced intergranular corrosion in both the fin and the wick. Recommendations for alleviating the corrosion problem included reducing the heat flux, redesigning the wick, and reducing the oxygen content of the sodium.