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Intergranular corrosion
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Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c0091362
EISBN: 978-1-62708-220-4
Abstract
A nozzle in a wastewater vaporizer began leaking after approximately three years of service with acetic and formic acid wastewaters at 105 deg C (225 deg F) and 414 kPa (60 psig). The shell of the vessel was weld fabricated from 6.4 mm (0.25 in.) E-Brite stainless steel plate and measured 1.5 m (58 in.) in diameter and 8.5 m (28 ft) in length. Investigation (visual inspection, chemical analysis, radiography, dye-penetrant inspection, and hydrostatic testing of all E-Brite welds, 4x images, 100x/200x images electrolytically etched with 10% oxalic acid, and V-notch Charpy testing) supported the conclusion that failure of the nozzle weld was the result of intergranular corrosion caused by the pickup of interstitial elements and subsequent precipitation of chromium carbides and nitrides. Carbon pickup was believed to have been caused by inadequate joint cleaning prior to welding. The increase in the weld nitrogen level was a direct result of inadequate argon gas shielding of the molten weld puddle. Two areas of inadequate shielding were identified: improper gas flow rate for a 19 mm (0.75 in.) diam gas lens nozzle, and contamination of the manifold gas system. Recommendations included changes in the cleaning and welding process.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001402
EISBN: 978-1-62708-220-4
Abstract
Weld-decay and stress-corrosion cracking developed in several similar all-welded vessels fabricated from austenitic stainless steel. During a periodic examination cracks were revealed at the external surface of one of the vessels. External patch welds had been applied at these and several other corresponding locations. Cracks visible on the external surface developed from the inside in a region close to the toe of the internal fillet weld to the deflector plate, and another deep crack associated with a weld cavity is visible slightly to the right of the main fissure. Microscopic examination revealed that precipitation of carbides at the grain boundaries had taken place in the vicinity of the cracks, but that the paths of the cracks were not wholly intergranular. Conditions present in the vicinity of the internal fillet weld must have been such as to favor both inter- and transgranular cracking. It is probable that the heating associated with the repair welds made from time to time also contributed to the trouble. The transgranular cracks, however, were indicative of stress-corrosion cracking.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001213
EISBN: 978-1-62708-220-4
Abstract
Fragments of screen bars which as structural elements of a condenser had come into contact with cooling water from the mouth of a river were received. The screen bars were made of stainless austenitic Cr-Ni-Mo steel X 5 Cr-Ni-Mo18 10 (Material No. 1.4401). The bars were fractured repeatedly. The ruptures did not occur exclusively or even preferentially at the loops, but just as frequently at locations between them. The mistake made in this case was annealing the steel at a temperature in the critical region. This was probably done to relieve stresses that originated during cold-forming and led to damage by stress corrosion. This would have been the correct method for a ferritic steel, but not austenitic steel, which requires the special heat treatment indicated. When an anneal in the critical region is unavoidable and the indicated additional treatment is impossible or difficult, a type of steel has to be chosen which is resistant to intergranular corrosion.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.chem.c9001395
EISBN: 978-1-62708-220-4
Abstract
Leakage which developed from two storage vessels handling a mixture of trimethyl formate and chloroform took place from the dished head at the edge of the circumferential weld to the shell which incorporated a backing ring. Some shallow pitting had occurred under the backing ring on the shell side behind the tack welds securing the backing strip to the shell. Intermittent pitting had also occurred along the head side of the weld at the other end the vessel. There was no pitting along the main longitudinal weld of the shells in any vessel nor around any of the branches set into the shells. The material of the original vessels was specified as BS 970 - 1966. En 58J. Sections taken through pitted areas from both head welds showed preferential attack along the grain-boundaries, some grains becoming completely detached. The location of the pitting and preferential attack was at such a distance from the weld that the heat of welding could have raised the metal temperature to 550 to 700 deg C (1292 deg F). The corrosion of the shell material which occurred at the shell side of the weld under the backing ring is also an example of crevice corrosion.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0091655
EISBN: 978-1-62708-229-7
Abstract
Cracking occurred in an ASME SB166 Inconel 600 safe-end forging on a nuclear reactor coolant water recirculation nozzle while it was in service. The safe-end was welded to a stainless-steel-clad carbon steel nozzle and a type 316 stainless steel transition metal pipe segment. An Inconel 600 thermal sleeve was welded to the safe-end, and a repair weld had obviously been made on the outside surface of the safe-end to correct a machining error. Initial visual examination of the safe-end disclosed that the cracking extended over approximately 85 deg of the circular circumference of the piece. Investigation (visual inspection, on-site radiographic inspection, limited ultrasonic inspection, chemical analysis, 53x metallographic cross sections and SEM images etched in 8:1 phosphoric acid) supported the conclusion that the cracking mechanism was intergranular SCC. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c0048299
EISBN: 978-1-62708-229-7
Abstract
Pendant-style reheater, constructed of ASME SA-213, grade T-11, steel ruptured. A set of four tubes, specified to be 64 mm OD x 3.4 mm minimum wall thickness was examined. A small quantity of loose debris was removed from the inside of one of the tubes. The major constituent was revealed by EDS analysis of the debris to be iron with traces of phosphorus, manganese, sodium, calcium, copper, zinc, potassium, silicon, chromium, and molybdenum. Thus the debris was interpreted to be the scale from ID of the tube with boiler feedwater chemicals from the attemperation spray. The likely cause of failure was concluded to be exfoliation of the scale from the ID surface of the tube. Creep failures were interpreted to be caused by localized temperatures higher than the maximum service temperature. Replacement of the affected tubes was recommended. Inspection of the tubes by radiography to find the circuits with the greatest accumulation of debris and replacing them as necessary was recommended on an annual basis.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001651
EISBN: 978-1-62708-229-7
Abstract
Some of the admiralty brass tubes were failing in a heat exchanger. The heat exchanger cooled air by passing river water through the inside of the tubes. The wall thickness of all tubes ranged between 1.19 to 1.27 mm (0.047 to 0.050 in.). General intergranular corrosion occurred at the inside surfaces of the tubes. Transgranular stress-corrosion cracking, probably the result of sulphates under basic conditions, and dezincification occurred also as the result of galvanic corrosion under the deposits in the tubes. Recommendations were to use a closed-loop water system to eliminate sulphates, ammonia, etc., and to run trials on one unit with tubes of other alloys such as 80-20 Cu-Ni or 70-30 Cu-Ni to evaluate their performance prior to any large scale retubing operations.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001710
EISBN: 978-1-62708-229-7
Abstract
Aluminum-clad spent nuclear fuel is stored in water filled basins at the Savannah River Site awaiting processing or other disposition. After more than 35 years of service underwater, the aluminum storage racks that position the fuel bundles in the basin were replaced. During the removal of the racks from the basin, a failure occurred in one of the racks and the Savannah River Technology Center was asked to investigate. This paper presents the results of the failure analysis and provides a discussion of the effects of corrosion on the structural integrity of the storage racks.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.power.c9001666
EISBN: 978-1-62708-229-7
Abstract
Stress-corrosion cracking of low-alloy steel turbine discs has emerged as a generic concern in nuclear generating stations. An investigation that made extensive use of field metallographic techniques to examine suspected cracking in such a component is described. The crack position, and its relationship to surface topographic features, were examined and recorded by magnetic rubber and high-resolution dental rubber replicating materials. Corrosion deposits on keyway surfaces and within the crack were collected with acetate foil replicas applied and then stripped from the keyway surfaces. Microstructural details were revealed by the use of field metallographic preparation techniques and replicated by acetate foil for examination with optical and scanning electron microscopes. It was possible by these techniques to establish the cracking mechanism as stress corrosion possibly related to chloride or sulphate ion steam contaminants. Subsequent sectioning and conventional metallography confirmed both the validity of the conclusions and the replication techniques.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c0089682
EISBN: 978-1-62708-230-3
Abstract
A neck fitting (cast equivalent of AISI type 317) exhibited extreme corrosion with large, deeply pitted areas. It had been in service in a sulfite digester at 140 deg C (285 deg F) and 689 kPa (100 psi). The liquor was calcium bisulfite, and chloride content was reported to be low. Investigation (visual inspection, and micrographs of sections with electrolytic etching using 10 N KOH and then again after re-polishing and etching with Murakami's reagent) supported the conclusions that the casting never received a proper solution anneal. Recommendations included possible corrosion-screening tests in accordance with ASTM A 262 to ensure adequate corrosion resistance.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.pulp.c9001563
EISBN: 978-1-62708-230-3
Abstract
An Inconel-clad SA-212 Grade B carbon steel inlet cone with an anticipated 25-year service life failed in a localized area after only seven years of service. The failure was caused by an erosion/corrosion leak at the midsection. Erosion/corrosion was confined to a localized area directly facing the steam inlet nozzle. The Inconel cladding was intact elsewhere in the inlet cone with insignificant corrosion-related degradation. In the absence of the conditions that led to erosion/corrosion, the Inconel clad carbon steel was considered adequate for the intended service. As a corrective measure, a solid Inconel liner was recommended in the areas of direct steam impingement.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001548
EISBN: 978-1-62708-219-8
Abstract
In 1975, a manufacturer was awarded a contract to produce modular air-traffic control towers for the U.S. Navy. The specifications called for painted steel siding, but the manufacturer convinced the Navy to substitute aluminum-bonded-to-plywood panels that were provided by a supplier. In less than one year, the panels began to delaminate and the aluminum began to crack. It was found that the failure was the result of chloride-induced intergranular corrosion caused by chemicals in the adhesive and excessive moisture in the wood introduced during manufacturing.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.bldgs.c9001171
EISBN: 978-1-62708-219-8
Abstract
The defects observed along weldings of stainless steel pipelines employed in marine environments were evidenced by metallographic and electrochemical examination. A compilation of cases on the effect of defective weldings, in addition to improper choice of stainless steel for water pipelines, lead to the conclusion that intercrystalline corrosion in steels involved precipitation of a surplus phase at grain boundaries. Intercrystalline corrosion in austenitic stainless steels due to precipitation of chromium carbides during conditions generated due to welding and ways to avoid the precipitation (including reduction of carbon content, appropriate heat treatment, cold work of steel, reduction of austenitic grain size and stabilizing elements) were described. The presence of microcracks due to highly localized heat concentrations with consequent thermal expansion and considerable shrinkages during cooling was investigated. The specimens were taken from various sources including transverse and longitudinal welding seam, sensitized areas and it was concluded appropriate material selection with respect to medium could control some corrosion processes.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.usage.c9001599
EISBN: 978-1-62708-236-5
Abstract
Failure of a pilot scale test melter resulted from severe overheating of an Inconel 690 (690) jacketed molybdenum electrode. Extreme temperatures were required to melt the glass during this campaign because the feed material contained a very high waste loading. Metallurgical evaluation revealed the presence of an alloy containing nickel and molybdenum in several ingots found on the bottom of the melter and on a drip which had solidified on the electrode sheath. This indicates that a major portion of the electrode assembly was exposed to a temperature of at least 1317 deg C, the nickel/molybdenum eutectic temperature. Small regions on the end of the 690 sheath showed evidence of melting, indicating that this localized region exceeded 1345 deg C, the melting point of 690. In addition to nickel, antimony was found on the grain boundaries of the molybdenum electrode. This also contributed to the failure of the electrode. The source of the antimony was not identified but is believed to have originated from the feed material. Metallurgical evaluation also revealed that nickel had attacked the grain boundaries of the molybdenum/tungsten drain valve. This component did not fail in service; however, intergranular attack led to degradation of the mechanical properties, resulting in the fracture of the drain valve tip during disassembly. Antimony was not observed on this component.
Book Chapter
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.process.c0047453
EISBN: 978-1-62708-235-8
Abstract
The origins of the casting are unknown. It is included here as a classic case of intergranular corrosion. The part (apparently a pump outlet) was named the “rubber casting” because of the severity of the intergranular attack. Every grain boundary has been attacked to the extent that the casting could be twisted and stretched as through made of rubber. The chemistry of the casting was acceptable for CN-7M. The reason the part failed is a continuous film of carbide with a continuous crack running parallel to the carbides. This sensitized structure produces an area depleted in protective chromium, making it susceptible to corrosion. Two solutions to this problem are available. The simplest is to ensure correct heat treatment to dissolve grain-boundary carbide film and return the protective chromium to the depleted zone. Alternatively, a low-carbon (0.03% maximum C, for example, CF-3) grade can be specified. Procedures are given in a reference for screening castings that may be susceptible to intergranular corrosion due to processing errors.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.med.c0048400
EISBN: 978-1-62708-226-6
Abstract
Cerclage wire, which was used with two screws and washers for a tension band in a corrective internal fixation, was found broken at several points and corroded after nine months in service. The material was examined using energy-dispersive x-ray analysis and determined not to be in compliance with standards (type 304 stainless steel without molybdenum). The screws and washers were found to be made of remelted implant-quality type 316L stainless steel and were intact. Signs of sensitization, characterized by chromium carbide precipitates at the grain boundaries, were revealed by the microstructure. Intercrystalline corrosion with pitted grains was indicated by SEM fractography. Improper heat treatment of the steel was interpreted to have led to intercrystalline corrosion and implant separation.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c9001223
EISBN: 978-1-62708-233-4
Abstract
The corner of a welded sheet construction made from austenitic corrosion-resistant chromium-nickel steel showed corrosive attack of the outer sheet. This attack was most severe at the points subjected to the greatest heat during welding. Particularly large amounts of weld metal had been applied. Microscopic examination showed grain disintegration was promoted by the thickness of the weld bead and the amount of heat required to produce it. If nonstabilized austenitic sheet is to be used in the future, one of the particularly low-carbon steels, X2 CrNi 18 9 or X2 CrNiMo 18 10, is recommended.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.design.c0091358
EISBN: 978-1-62708-233-4
Abstract
After about two years in service, a 303 stainless steel valve in contact with a carbonated soft drink in a vending machine occasionally dispensed a discolored drink with a sulfide odor. According to the laboratory at the bottling plant, the soft drink in question was strongly acidic, containing citric and phosphoric acids and having a pH of 2.4 to 2.5. Investigation (visual inspection, chemical analysis, immersion testing in the soft drink, and 100x unetched micrographs) supported the conclusion that the failure was caused by the size and distribution of sulfide stringers in the alloy used in the valve. Manganese sulfide stringers in the valve were exposed at end-grain surfaces in contact with the beverage. The stringers, which were anodic to the surrounding metal, were subject to corrosion, producing a hydrogen sulfide concentration in the immediately adjacent liquid. Recommendations included changing the valve material to type 304 stainless steel.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c0091350
EISBN: 978-1-62708-227-3
Abstract
Cracks occurred in a new ship hull after only three months in service. It was noted that the 5xxx series of aluminum alloys are often selected for weldability and are generally very resistant to corrosion. However, if the material has prolonged exposure at slightly elevated temperatures of 66 to 180 deg C (150 to 350 deg F), an alloy such as 5083 can become susceptible to intergranular corrosion. Investigation (visual inspection, corrosion testing, SEM images) supported the conclusion that the cracks occurred because during exposures to chloride solutions like seawater, galvanic couples formed between precipitates and the alloy matrix, leading to severe intergranular attack. No recommendations were made.
Series: ASM Failure Analysis Case Histories
Publisher: ASM International
Published: 01 June 2019
DOI: 10.31399/asm.fach.marine.c9001164
EISBN: 978-1-62708-227-3
Abstract
Plate perforation occurred in the cylindrical section and walls of the inlet foot (2.38 mm thick Incoloy 825 plate welded using INCO welding rod 135) of an inert gas fire prevention system in an oil tanker. Cross-sectional microprobe analysis showed the corrosion product to contain sulfur, mainly from the flue gas, and calcium and chlorine, mainly from the sea water. The gray corrosion product was interspersed with rust and a black carbonaceous deposit. Corrosion pitting and poor weld penetration, with carbide precipitation and heavy etching at grain boundaries, indicated sensitization and susceptibility to aqueous intergranular corrosion. Chemical analysis showed the predominant acid radical to be sulfate (6.20% in the carbonaceous deposit and 0.60% in the corrosion product), suggesting that oxidation of SO2 in the flue gas caused the corrosion. Moisture condensation, the carbon acting as a cathode, and alloy susceptibility to intergranular corrosion contributed to the corrosion.
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