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The horizontal cross-travel shaft on a derrick failed after two years of service. The shaft was required to be made of 4140 steel quenched to a hardness of 302 to 352 HRB. The shaft was found to have fractured approximately 13 mm from the change in section between the splined end and the shaft proper. The cracks were found to have propagated in the longitudinal and transverse directions until failures occurred. It was showed by a transverse section through the spline that the longitudinal cracks were initiated at the sharp corners at the roots of the spline teeth. The shaft was subjected to reverse torsional loading by the operation of the derrick and the shaft fatigue fracture was caused by this. The fillets at the roots of the spline teeth were increased in size and polished to minimize stress concentrations in these areas.

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