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Two clevis-head self-retaining bolts used in the throttle-control linkage of a naval aircraft failed on the aircraft assembly line. Specifications required the bolts to be heat treated to a hardness of 39 to 45 HRC, followed by cleaning, cadmium electroplating, and baking to minimize hydrogen embrittlement. The bolts broke at the junction of the head and shank. The nuts were, theoretically, installed fingertight. The failure was attributed to hydrogen embrittlement that had not been satisfactorily alleviated by subsequent baking. The presence of burrs on the threads prevented assembly to finger-tightness, and the consequent wrench torquing caused the actual fractures....

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