This paper reports the results of a collaborative investigation of an ex-service grade 91 bend carried out by the UK generating companies Centrica, SSE, Engie and RWE. As part of the handover exercise for Centrica’s Langage power station in 2009 a number of routine checks were carried out on the main steam and hot reheat grade 91 steam pipework. In some cases low hardness readings were found with subsequent metallurgical replication showing the presence of an aberrant non martensitic microstructure. This led to a more extensive inspection programme on the steam lines and the discovery of other areas of suspect material. A review of the operating capability of the plant, including detailed pipework stress analysis and a pipework peaking assessment, along with the assumption that lower strength grade 91 material was present, led to the steam lines being down rated and returning to service under these revised conditions. At the first C inspection in December 2012, after the HRSG and associated pipework had operated for 18720 hours, a bend with a soft weld, along with a section of the straight pipe on either side, was removed from service. An investigation was undertaken to establish how long this component would have survived, had it been left in service, and to consider the implications for the future operation of the plant.

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