The mechanisms of recent cracking failures of HR3C super heater pipes of a fossil power plant in the Netherlands were investigated. Initial failure investigations showed that pitting corrosion of the sensitized HR3C initiated subsequent stress corrosion cracking (SCC). It was concluded that magnesium chloride hydrates from condensed seawater had initiated pitting corrosion as well as SCC similar to the standard ASTM G36 SCC test. By experimental application of the ASTM G36 procedure, this tentative mechanism is reproduced and confirmed by a series of laboratory tests with pure magnesium chloride as well as with synthetic seawater. It included the effects of temperature, magnesium chloride concentrations of the evaporating water and applied bending moments on cracking. As a result for the 175h testing period in MgCl2*6H2O cracking increases significantly above 100°C up to 120°C but is reduced slightly at temperatures up to 155°C. With increasing bending moments, the U-shaped test pieces revealed increasing crack depths up to total fracture of the 5mm thick sections. Lower magnesium chloride concentrations as in concentrated seawater provided identical cracking, however, to a lower extent. It is therefore concluded that the operational failure of the sensitized HR3C super heater pipes was initiated in presence of condensed seawater and followed the same mechanism as found in the experimental investigation. As a conclusion, the presence of seawater saturated air at temperatures between 100° and 155°C should be avoided.

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